QFR No - 7000822416
Defect Details
NC No. 7000822416
NC Date 03/03/2022
NC Submission Date
Part No. S2PL01307B
Part Name WASHER
Supplier Name & Code 100299-CITIZEN EXPORTS
ETL Plant 1126-ETL Pantnagar
Defect Details DIMETER UNDERSIZE-Diameter Undersize.
 
1. Problem Description
Defect Description I/D undersize in Washer P/C B104E (S2PL01307B) - I/D Specification : 28.10 + 0.20 mm & I/D Observation : 27.88 mm.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 2000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualitypantnagar@citizencomponents.com
Plant Head/CEO Email ID citizenexports@citizencomponents.com
MD Email ID ceo@citizencomponents.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7850
0
0
6500
0
14350
Check Qty
7850
0
0
6500
0
14350
NG Qty
2000
0
0
120
0
2120
 
Scrap 0
Rework 2120
Under Deviation 0
Containment Action
100% Part Checked at Customer end & our FG & WI Stage and after inspection put a dot marking on part with white paint marker .
 
3. Process Flow
Process Flow Description
Hole ID Punching (Blanking & Punching )
 
4. Process Details
Process / Operation Blank & Punching
Outsource No
Machine / Cell Power Press Machine
Machine / Cell No. 75Ton -02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Mantrained OperatorOperator aware about the ID specification for washerO
ToolTool Punch ok as per requiredTool Punch observed in lower side as per requiredX
MethodAfter Powder coating part ID inspectionAfter Powder coating part ID inspection on sampling base (5 no`s/Lot)O
MaterialMaterial Grade or Thickness as per drawingMaterial Grade or Thickness is ok as per drawingO
MachineMachine capacity75 Ton machine to maintain part thickness & OD of the partO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 Nos /L
7. Root Cause Analysis (Occurance)
Why 1 Washer ID Observed under size -27.88 mm against 28.10+0.2mm.
Why 2 Tool Punch diameter observed 28 mm, lower than the specification of part ID
Why 3 Tool wear out before the set life of 50K no`s
Why 4 No daily verification of tool condition & part ID during process set up
Why 5
Root Cause (Occurance) No daily verification of tool condition & part ID during process set up
 
Root Cause Analysis (Outflow)
Why 1 Washer ID not as per specification after powder coating
Why 2 Defective parts not arrested during inspection
Why 3 Checking only 5 No`s during final stage
Why 4 Final process not designed to arrest defective parts
Why 5
Root Cause (Outflow) NG Part not found during sampling inspection due to less sample size (5 no`s/ Lot)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool Punch Outer Diameter 28.30 ~28.40mm will checked during process setup in FPPIMr. Jaswant Singh & Mr. Vineet Kumar07/03/202220/04/2022Completed
OccuranceNew Tool Punch designed consider powder coating process 28.40mmMr. Amrish Sharma07/03/202220/04/2022Completed
Outflow100% Part Will checked after powder coating with ID plug gauge before dispatch at quality gateMr. Yogesh Kumar07/03/202220/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection done after Powder coating before Dispatch for 1Month at Quality Gate
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size per Lot
10. Evidance of Countermeasure
Occurance (Before) 1-NO daily verification of tool condition during setup approval 2- Punch ID under Size as per Required 0.35mm.
3_Occurance_Before.pptx
Occurance (After) 1- Daily verification started of tool condition during setup approval 2- New ID punch provided 28.45mm and part ID observation 28.18~28.25mm after P/C.
3_Occurance_After.pptx
Outflow (Before) Sampling Inspection done by instruments (DVC)
3_Outflow_Before.pptx
Outflow (After) 1- 100% Inspection done with ID checking gauge and after Inspection dot marking done on part with white paint marker
3_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant 533PL00207 Washer / ETL Suspension
 
12. Document Review
Documents ControlPlan
Specify Other Document Not changed
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Ok