QFR No - 7000823246
Defect Details
NC No. 7000823246
NC Date 07/03/2022
NC Submission Date
Part No. 520AE00100
Part Name CORE PLATE CAL 115
Supplier Name & Code 101145-STAR PROJECTS INDIA
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details FLATNESS NOT OK.-Flatness o/s 0.25~0.30 mm against 0.10
 
1. Problem Description
Defect Description Flatness oversize upto 0.25~0.30 mm against 0.10 mm
Detection Stage Receipt
Problem Severity Function
NG Quantity 6000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityhead@starprojectsindia.com
Plant Head/CEO Email ID engineering@starprojectsindia.com
MD Email ID ishant@starprojectsindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6000
192000
0
12000
0
210000
Check Qty
6000
36000
0
12000
0
54000
NG Qty
6000
0
0
0
0
6000
 
Scrap 6000
Rework 0
Under Deviation 0
Containment Action
All material has been hold for 100% re-inspection the same with proper identification
 
3. Process Flow
Process Flow Description
Receipt of raw material- storage of raw material-Melting-PDC-1st Trimming -Shot blastng-2nd trimming-Barrelling-Shot blasting-Sound testing-Stress relieving -Final inspection & Packing-Storage & Dispatch
 
4. Process Details
Process / Operation Packing & Dispatch
Outsource No
Machine / Cell Final inspection & Packing
Machine / Cell No. Packing
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodPoor handling during transitCorrugated box of 5 ply using for packing ,chance of flatness issueX
Method100% receiving gauging not done or gauge wear out100% gauging process done and also gauge verification doing as per defined frequency (F07/QAD(JFR)O
MethodHeating process not done properlyHeating process adhered as per instruction (WI / PRM / 005,,F10/PRM(OLUM)O
MethodPart not interlock with each other in heating fixture during heating processPart proper locked in fixture at heating process by keshavO
ManunskilledUday pratap ,Baijnath was aware about the flatness issueO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Per Lot
7. Root Cause Analysis (Occurance)
Why 1 Poor handling during transit ,chance of flatness issue
Why 2 Existing Packing box not enough to avoid bend or flatness issue during transit .
Why 3 No provision available in existing (Corrugated 5 ply) box to avoid flatness issues during transit.
Why 4 Flatness & broken possibility not consider during material handling in transit
Why 5
Root Cause (Occurance) Flatness & broken possibility not consider during material handling in transit
 
Root Cause Analysis (Outflow)
Why 1 Check point not available at warehouse for flatness /Bend issue in core plate
Why 2 Flatness & bend issue not considered while defined control plan
Why 3 No criteria for defining the inspection parameters in control plan
Why 4
Why 5
Root Cause (Outflow) No criteria for defining the inspection parameters in control plan
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePP corrugated foldable box to be introduced to avoid flatness and broken issue during transitBhim Singh25/04/202213/04/2022Completed
OccuranceSeparator sheet to be introduced in box at top & bottom side to avoid bend & broken issue during transitBhim Singh03/12/202212/03/2022Completed
Outflow100% marking started after inspection at warehouseBhim Singh12/03/202212/03/2022Completed
Outflowverification Check point to be added at warehouseBhim Singh03/12/202212/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% marking after gauging & inspection check point added at warehouse
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size each lot
10. Evidance of Countermeasure
Occurance (Before) 5 ply corrugated box using for core plate packing ,No separator available at bottom & top side ,Change of damage & flatness out issue .
5_Occurance_Before.pdf
Occurance (After) 1. 5 ply extra corrugated sheet provided in box at bottom & top side to avoid Flatness , broken & damage issue in core plate of K70 and as well as in other core plate . 2. PP Corrugated foldable box introduced instead of corrugated box 5 ply to avoid flatness ,Broken & damage issue during transit.
5_Occurance_After.pdf
Outflow (Before) 1. No check point available at warehouse .
5_Outflow_Before.pdf
Outflow (After) 1. Check point added with 100% marking after inspection at warehouse to detect flatness ,broken & damages issue in core plate
5_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant In all model of core plate
 
12. Document Review
Documents WISOP, PackingStd
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 50000
Reason for submission ok