QFR No - 7000824219
Defect Details
NC No. 7000824219
NC Date 10/03/2022
NC Submission Date
Part No. 165FY00422
Part Name HUB CLUTCH 3W4S MACHINED & BROACHED
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DIMETER UNDERSIZE-minor dia u/s plug not qualify
 
1. Problem Description
Defect Description Minor dia u/s plug not qualify
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 12
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1350
0
0
500
800
2650
Check Qty
1350
0
0
500
800
2650
NG Qty
12
0
0
2
0
14
 
Scrap 14
Rework 0
Under Deviation 0
Containment Action
1.100% Stock segregate at customer end and Supplier end stock.
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Broaching 6.Final Inspection
 
4. Process Details
Process / Operation Broaching
Outsource No
Machine / Cell BROACHING
Machine / Cell No. MDCPL/BROACHING/01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodComponent was not proper kept on broaching fixture.Broaching fixture checked and verify found okO
ManUnskilled operator operated machineSkill matrix plan verify operator is skillful foundO
ToolBroach tool life monitoring not effectively monitorTool life monitoring sheet not available.X
MaterialHard point impurity material is used for broachingComponent checked found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 1 : 5
7. Root Cause Analysis (Occurance)
Why 1 Broch wear
Why 2 Broach Reshaping not done as per decided frequency
Why 3
Why 4
Why 5
Root Cause (Occurance) 1.Broch wear 2.Broach tool life not monitor
 
Root Cause Analysis (Outflow)
Why 1 Inspection frequency is less
Why 2 unskilled inspector
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection frequency is less
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1. Inspection frequency of minor dia by plug gauge increasesQA.Supervisor04/01/2022Completed
Occurance1.Tool life monitoring incorporated in Broaching machine. 2.Broach tool monitoring sheet is available and verify by production supervisorProduction Supervisor04/01/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Minor dia checking and final inspection by plug gauge on sampling bases and started 100% by plain plug gauge
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:5
10. Evidance of Countermeasure
Occurance (Before) Broach wear broach life not effectively monitored as per decide frequency
12_Occurance_Before.jpeg
Occurance (After) Broach life monitoring started as per decide frequency & start verifying pokayoke verification sheet on weekly basis for broach machine counter
12_Occurance_After.pdf
Outflow (Before) Inspection Frequency less 01:05 on sampling basis
12_Outflow_Before.pdf
Outflow (After) Control plan updated at final inspection stage for minor dia inspection started 100% by plain plug gauge
12_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Broach Machine
 
12. Document Review
Documents ControlPlan, PokayokeCheckSheet, InspCheckSheet
Specify Other Document Broach life sheet
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission There is one system we have implemented to monitor broach tool life why it was bypassed pl give explanation and action on same