QFR No - 7000827149
Defect Details
NC No. 7000827149
NC Date 23/03/2022
NC Submission Date
Part No. 533KU00102
Part Name ROD GUIDE
Supplier Name & Code 204749-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1126-ETL Pantnagar
Defect Details NOT AS PER SPECIFICATION-Chamfer profile not OK
 
1. Problem Description
Defect Description Chamfer profile not OK - Step observed at chamfer of Rod guide (533KU00102)
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 5000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Bhaskar.Dhalawade@gknpm.com
Plant Head/CEO Email ID Purushottam.Rishi@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
25000
0
0
0
30000
Check Qty
5000
25000
0
0
0
30000
NG Qty
5000
25000
0
0
0
30000
 
Scrap 0
Rework 30000
Under Deviation 0
Containment Action
Part can not be reworked at WH or Customer end , all parts ( 30K) called back for rework at GKN end
 
3. Process Flow
Process Flow Description
Mixing > Forming > sintering > Barreling > Chamfering > Sizing > 100% inspection > oil dipping > Final inspection > dispatch
 
4. Process Details
Process / Operation Sizing
Outsource No
Machine / Cell K40
Machine / Cell No. Szing_ K40 Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineTool alignment issuesSizing die, top punch, bottom punch, core rod clearance checked and found within 0.020mm ( OK)X
MachineFree flow of material at inclind chamfer face during sizing processChamfer profile check by contour graph tracing ; curvature observed on chamfer faceO
MethodChamfer profile not checked in sizingVrified control plan for chamfer angle check ; chamfer angle is checked in chamfering process howeveO
ManUnskilled operatorSkill matrix verified ; found OKX
MachineChamfering tool worn outChanfering core rod inspected and found OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2
7. Root Cause Analysis (Occurance)
Why 1 Curvature shape profile of C`bore chamfer causes sharp edge at the end of chamfer
Why 2 Free flow of material at incline chamfer face during sizing process
Why 3 Chamfer area not supported by tool at incline portion in sizing process
Why 4 Degree not provided on sizing tool while sizing
Why 5
Root Cause (Occurance) Degree not provided on sizing tool while sizing
 
Root Cause Analysis (Outflow)
Why 1 Abnormal profile of core rod could not get detected during sizing inspection
Why 2 Abnormal chamfer in sizing process not detected by inspector
Why 3 Chamfer not checked by inspector in sizing process
Why 4 Chamfer check not mentioned in sizing QC ( Only checked in chamfering process)
Why 5
Root Cause (Outflow) Chamfer check not mentioned in sizing QC ( Only checked in chamfering process)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow. Control plan to be updated for adding chamfer inspection during sizing operationAjay Shinde08/04/2022Completed
Occurance2. Core rod design to be modified : chamfer profile to given on core rod instead of using plain core rod.Ajay Shinde08/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details chamfer degree inspection during sizing operation
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2 / batch
10. Evidance of Countermeasure
Occurance (Before)
Occurance (After)
Outflow (Before)
Outflow (After)
 
11. Horizontal Deployment
Horizontal Deployment Required
Applicable Machine / Model / Plant
 
12. Document Review
Documents
Specify Other Document
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission