QFR No - 7000828626
Defect Details
NC No. 7000828626
NC Date 29/03/2022
NC Submission Date
Part No. F2DZ08810B
Part Name K0PG FORK BOLT
Supplier Name & Code 101037-SHREE PATEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details SALT SPRAY TEST FAIL-SST Failed in 48 Hours
 
1. Problem Description
Defect Description SST Failed i.e. Heavy White Rust formation observed at part within 48 Hours against the 72 Hours No White Rust formation.
Detection Stage Receipt
Problem Severity Function
NG Quantity 2159
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality_spi@rediffmail.com
Plant Head/CEO Email ID planthead_spi@rediffmail.com
MD Email ID rspatel_spi@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
0
0
3000
Check Qty
3000
0
0
0
0
3000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Hold the material at final inspection & plating.
 
3. Process Flow
Process Flow Description
10.Incoming RM 20. Traub Turning 30. CNC 1st set up 40. CNC 2nd set up 50. Plating 60. Inspection 70. Packing & Dispatch
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell Plating M/C
Machine / Cell No. Plating M/C No.-1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachinePassivation bath tankDuring process verification passivation bath tank capacity found changeO
MaterialPlating PassivationDuring process verification plating passivation pH found dropO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
7. Root Cause Analysis (Occurance)
Why 1 Heavy rust observed during SST at customer end.
Why 2 Plating passivation found improper .
Why 3 Passivation PH Drop
Why 4 Passivation tank found leakage & replaced with new one with increased capacity (20 Ltr to 25 ltr)
Why 5 Daily passivation top up chemical was fixed as per 20 ltr bath tank.(50gm/ltr)
Root Cause (Occurance) Passivation tank found leakage & replaced with new one with increased capacity (20 Ltr to 25 ltr)
 
Root Cause Analysis (Outflow)
Why 1 Heavy rust observed during SST at customer end.
Why 2 Inspector not detected dull plated part during final inspection .
Why 3 Inspector was not aware about the defect.
Why 4 No inspection std available at final inspection station
Why 5
Root Cause (Outflow) No inspection std available at final inspection station
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1.Daily passivation top up chemical maintain as per new bath tank (From 1.0 ltr to 1.25 ltr) 2. Top coated chemical also maintain as per new bath tank (From 1.0 ltr to 1.25 ltr) . 3. Material send for SST testing , result awaitedPradeep tripathi17/06/2022Pending
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
10. Evidance of Countermeasure
Occurance (Before) WI
32_Occurance_Before.xlsx
Occurance (After) WI
32_Occurance_After.xlsx
Outflow (Before) Sampling Plan
32_Outflow_Before.xls
Outflow (After) Sampling Plan
32_Outflow_After.xls
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents WISOP
Specify Other Document Sampling Plan
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission