QFR No - 7000829350
Defect Details
NC No. 7000829350
NC Date 02/04/2022
NC Submission Date
Part No. F2DZ08810B
Part Name K0PG FORK BOLT
Supplier Name & Code 100189-SANGKAJ STEEL PVT LTD.
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIMETER UNDERSIZE-Grove Dia 22.45-0.1 found Under Size
 
1. Problem Description
Defect Description Grove Dia NG ( Under Size & Over Size)
Detection Stage Receipt
Problem Severity Function
NG Quantity 2400
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID maheshmishra@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2400
0
0
2000
2000
6400
Check Qty
2400
0
0
2000
2000
6400
NG Qty
2400
0
0
0
0
2400
 
Scrap 0
Rework 2400
Under Deviation 0
Containment Action
100% material inspect at my end blue identification mark provided on component. also material started 100% checking with snap gauge.
 
3. Process Flow
Process Flow Description
RM INWARD - PARTING - TURNING CNC1 - TURNING CNC2 - PLATING - FINAL INSPECTION - DISPATCH
 
4. Process Details
Process / Operation CNC TURNING 2ND SETUP
Outsource No
Machine / Cell CNC MACHINE CELL
Machine / Cell No. 38
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodINSERT WEAR OUT AND DOUBLE PUNCHINSERT DOUBLE PUNCHX
MethodINSERT LIFE NOT MONITORINGINSERT LIFE MONITORED FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50
7. Root Cause Analysis (Occurance)
Why 1 Grove OD undersize.
Why 2 Insert double plunge for 3.10 mm slot making purpose.
Why 3 Standard insert is not available
Why 4
Why 5
Root Cause (Occurance) Standard insert is not available so we punch insert 2 times in groove.
 
Root Cause Analysis (Outflow)
Why 1 Grove OD undersize.
Why 2 Not detected in inspection
Why 3 Material checked with snap gauge.
Why 4
Why 5
Root Cause (Outflow) Material checked with snap gauge.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNow we used 3 mm insert and 0.1 mm we linear machining.Raut Santosh20/04/202226/04/2022Completed
Outflow100%c material inspect with Digital vernier and blue identification mark also providedMahesh Mishra20/04/202203/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Material 100 Inspect with Digital vernier against snap gauge.
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 00
10. Evidance of Countermeasure
Occurance (Before) Standard insert is not available so we plunge insert 2 times in groove.
40_Occurance_Before.jpg
Occurance (After) Now we used 3 mm insert and 0.1 mm we linear machining.
40_Occurance_After.jpg
Outflow (Before) Material 100% inspect with snap gauge
40_Outflow_Before.jpg
Outflow (After) Material 100% inspect with digital vernier
40_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 0
Reason for submission ETL Return Material stock details and actions are not given. All 4m to be addressed and fact verification to be corrected. Root Cause is not adequate (both Flow and Occurrence) i.e. why not detected at Setup inspection, Petro inspection sheet, PDIR etc. ? If tool double plunged then why 4M change not followed ? Occurrence side corrective action is given but preventive action is not defined i.e. How to avoid repeating of use of Non Standard tool. All Updated or Reviewed Documents to be uploaded (OPL, Training records, Control Plan etc.)