QFR No - 7000829982
Defect Details
NC No. | 7000829982 |
NC Date | 06/04/2022 |
NC Submission Date | |
Part No. | S2BY04007B |
Part Name | CANISTER M/C, IMPREGNATED & COATED |
Supplier Name & Code | 101032-ASM CASTINGS PRIVATE LIMITED ( |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | POWDER COATING NOT OK-POWDER COATING PEEL OFF |
1. Problem Description
Defect Description | Canister Failed in Adhesion Test at Receipt |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 2000 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | bxvtf0xyugvyhemmx3w43yva.png |
Supplier Communication Details
Quality Head Email ID | quality@asmcastings.in |
Plant Head/CEO Email ID | skaul@asmcastings.in |
MD Email ID | rajiv@asmcastings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1200
|
0
|
0
|
1650
|
1000
|
3850
|
Check Qty |
10
|
0
|
0
|
1650
|
1000
|
2660
|
NG Qty |
0
|
0
|
0
|
1650
|
0
|
1650
|
Scrap | 10 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Part Checked (10 Nos. each lot for Tape Test) and a chemical added in impregnation process as per M/S Ultraseal`s Recommendation (Sealant & Impregnation Unit Supplier) |
3. Process Flow
Process Flow Description |
---|
R.M. Receiving - Casting - Fattling- CNC Machining - SPM Machining- Impregnation - Pin Pressing - Leakage Testing- Dry in Oven - Inspection & PDI - Packing - Dispatch |
4. Process Details
Process / Operation | Impregnation |
Outsource | No |
Machine / Cell | Impregnation Unit |
Machine / Cell No. | N/A |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Ra not maintained from Shot Blasting Machine | Ra Inspection & Cycle Time Verification in Shot Blasting Machine | X |
Tool | Impregnation Unit not working adequately | Ring Test | X |
Material | Impregnation Sealant not effective | Impregnation done at Customer End with Other Brand | O |
Man | Operator not aware about process | Skill Matrix | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Tape Test |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | not detect |
7. Root Cause Analysis (Occurance)
Why 1 | Powder Coating Peel off at customer end |
Why 2 | bonding of Powder & Part could not be adequate |
Why 3 | a layer of chemical sealant deposited at surface of part |
Why 4 | Damaged /Old Mesh Used in Basket (mesh Not Changed Timely) |
Why 5 | Mesh Changing Freq. Not decided. |
Root Cause (Occurance) | Mesh Changing Freq. Not decided. |
Root Cause Analysis (Outflow)
Why 1 | Can Not detected at ASM |
Why 2 | Powder Coating at Outsource. (Customer /Supplier End) |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Powder Coating Out Source (Customer /Supplier) |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Qty. per Basket reduced from 600 nos. to 400 nos. per basket & added in Work Instruction. | Lalit Sharma | 30/07/2022 | 30/07/2022 | Completed |
Occurance | Awareness Training Provided to Concerned person for Work Instruction ammedment. | Lalit Sharma | 02/08/2022 | 02/08/2022 | Completed |
Occurance | Mesh Changing Freq. Added in Control Plan | Lalit Sharma | 01/02/2023 | Completed | |
Occurance | Sealant Grade Changed from PC504 to IM3000 to improve Impregnation Quality. | Ultraseal. | 28/10/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Supervisor Verification for part Qty. in Basket as per W.I. |
Inspection Method | Other |
Other Inspection Method | as per w.i. |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 10 |
10. Evidance of Countermeasure
Occurance (Before) |
01. Check Point not added in Work Instruction for qty per basket. 02. Sealent Grade Change from PC504 to IM3000 (Suggested by Impregnation Supplier) 47_Occurance_Before.png |
Occurance (After) |
Work Instruction Updated for Qty. per Basket 47_Occurance_After.pdf |
Outflow (Before) |
Awareness not evident to concern person for Qty. per basket. 47_Outflow_Before.jpg |
Outflow (After) |
Awareness Training provided to concerned person 47_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | n/a |
12. Document Review
Documents | WISOP |
Specify Other Document | W.I |
13. Effectiveness Of Action
Reviewed Quantity | 4000 |
Reason for submission | No any Peel Off Reported after Action Taken |