QFR No - 7000831525
Defect Details
NC No. | 7000831525 |
NC Date | 16/04/2022 |
NC Submission Date | |
Part No. | F2DZ08810B |
Part Name | K0PG FORK BOLT |
Supplier Name & Code | 101037-SHREE PATEL INDUSTRIES |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | DEEP MARK-Line Mark at OD 26.15 |
1. Problem Description
Defect Description | Line Mark at OD 26.15 |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1512 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality_spi@rediffmail.com |
Plant Head/CEO Email ID | planthead_spi@rediffmail.com |
MD Email ID | rspatel_spi@rediffmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
0
|
0
|
2618
|
0
|
12618
|
Check Qty |
10000
|
0
|
0
|
2618
|
0
|
12618
|
NG Qty |
1
|
0
|
0
|
2
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Hold the material at all stages and inspection done accordingly . |
3. Process Flow
Process Flow Description |
---|
1. Incoming RM 2. Acid Pickling 3. Water Wash 4. Lime Wash 5. Pointing 6. Draw 7. Cutting 8. Straightening 9. Inspection 10. Packing & Dispatch 11. Incoming RM 12. Traub Turning 13. CNC 1st Setup 14. CNC 2nd Setup 15. Plating 16. Inspection 17. Packing & Dispatch |
4. Process Details
Process / Operation | Draw |
Outsource | No |
Machine / Cell | Draw M/c |
Machine / Cell No. | Draw Line |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Awareness of Inspector | Inspector was not aware about inspection std. | O |
Machine | Die Check sheet | During process Verification no Die check point available. | O |
Machine | Die Life Monitoring | During process Verification no Die life monitoring record available. | O |
Method | Rod Draw | During process verification a deep line mark generated on rod during draw operation. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Deep Line mark part reached at customer end. |
Why 2 | Deep line mark part generate during CNC operation. |
Why 3 | Deep line mark found on input rod . |
Why 4 | At draw operation chips observed on rod, which remains a deep line on rod during draw process. |
Why 5 | There was No checkpoint & WI available at draw operation to check the input & output material of rod. |
Root Cause (Occurance) | At draw operation chips observed on rod which generate / remains a deep line on rod during draw operation |
Root Cause Analysis (Outflow)
Why 1 | Deep Line mark part reached at customer end. |
Why 2 | Inspector not detected deep line mark part during final inspection . |
Why 3 | Inspector was not aware about the defect. |
Why 4 | No inspection std available at final inspection station. |
Why 5 | |
Root Cause (Outflow) | No inspection std available at final inspection station. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1.WI made to check the Input & Output material & also FIR ,IIR made to check the draw bar after draw process . 2. Draw Die checkpoint check sheet made 3. Die life monitoring to be started . | Pradeep Tripathi | 18/02/2022 | 18/02/2022 | Completed |
Outflow | 1. Training provided to the final inspector about the problem and inspection std. 2. 200% visual inspection started. | Pradeep Tripathi | 18/02/2022 | 18/02/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 200% Visual Inspection |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Die Check sheet 55_Occurance_Before.zip |
Occurance (After) |
Die Check sheet 55_Occurance_After.zip |
Outflow (Before) |
Inspection std 55_Outflow_Before.xlsx |
Outflow (After) |
Inspection std 55_Outflow_After.zip |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | No |
12. Document Review
Documents | ControlPlan, PMCheckSheet, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |