QFR No - 7000833423
Defect Details
NC No. | 7000833423 |
NC Date | 27/04/2022 |
NC Submission Date | |
Part No. | 165PP01317 |
Part Name | WHEEL CLUTCH -4 PLATE VAVE |
Supplier Name & Code | 101100-CAST 4 ALUMINIUM PVT LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | PCD SHIFT-4Hole Lug Pcd Not ok |
1. Problem Description
Defect Description | 4 Hole Lug PCD Not ok |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 148 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | info@cast4aluminium.com |
Plant Head/CEO Email ID | info@cast4aluminium.com |
MD Email ID | kiran@cast4aluminium.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1560
|
0
|
0
|
2500
|
3000
|
7060
|
Check Qty |
1560
|
0
|
0
|
2500
|
3000
|
7060
|
NG Qty |
148
|
0
|
0
|
0
|
0
|
148
|
Scrap | 148 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Recheck all pipeline material to PCD gauge. |
3. Process Flow
Process Flow Description |
---|
Melting- casting- fettling- Inprocess inspection- CNC machining- 4 hole drilling and tapping- Final inspection- Packaging- Dispatch. |
4. Process Details
Process / Operation | 4 Hole drilling & tapping. |
Outsource | Yes |
Machine / Cell | VMC Machine |
Machine / Cell No. | VMC Machine |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | 1) 4 Lug Not qualify to PCD Gauge. 2) .Due to Fixture Clamping Loose One side. | Due to Fixture Clamping Loose One side. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | 4 Lug not qualify to PCD Gauge. |
Why 2 | Fixture Clamping Loose from one side. |
Why 3 | Due to this part not rest properly in fixture. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Fixture Clamping Loose from one side. |
Root Cause Analysis (Outflow)
Why 1 | 100 % inspection at final stage without marking. |
Why 2 | Operator knowledge not found evident. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | 100 % Inspection at Final stage without marking |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Proper Tight Clamping Fixture Both side. | Mr. Thakur. | 23/03/2022 | 23/03/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Start 100% inspection with identification marking. |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Fixture PM check sheet. 73_Occurance_Before.xlsx |
Occurance (After) |
Fixture PM check sheet & JH check sheet 73_Occurance_After.xlsx |
Outflow (Before) |
Without marking. 73_Outflow_Before.jpg |
Outflow (After) |
Inspection marking. 73_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Not applicable |
12. Document Review
Documents | PMCheckSheet, JHCheckSheet, InspCheckSheet |
Specify Other Document | Fixture check sheet. |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | OK |