QFR No - 7000833423
Defect Details
NC No. 7000833423
NC Date 27/04/2022
NC Submission Date
Part No. 165PP01317
Part Name WHEEL CLUTCH -4 PLATE VAVE
Supplier Name & Code 101100-CAST 4 ALUMINIUM PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details PCD SHIFT-4Hole Lug Pcd Not ok
 
1. Problem Description
Defect Description 4 Hole Lug PCD Not ok
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 148
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID info@cast4aluminium.com
Plant Head/CEO Email ID info@cast4aluminium.com
MD Email ID kiran@cast4aluminium.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1560
0
0
2500
3000
7060
Check Qty
1560
0
0
2500
3000
7060
NG Qty
148
0
0
0
0
148
 
Scrap 148
Rework 0
Under Deviation 0
Containment Action
Recheck all pipeline material to PCD gauge.
 
3. Process Flow
Process Flow Description
Melting- casting- fettling- Inprocess inspection- CNC machining- 4 hole drilling and tapping- Final inspection- Packaging- Dispatch.
 
4. Process Details
Process / Operation 4 Hole drilling & tapping.
Outsource Yes
Machine / Cell VMC Machine
Machine / Cell No. VMC Machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Method1) 4 Lug Not qualify to PCD Gauge. 2) .Due to Fixture Clamping Loose One side.Due to Fixture Clamping Loose One side.O
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 4 Lug not qualify to PCD Gauge.
Why 2 Fixture Clamping Loose from one side.
Why 3 Due to this part not rest properly in fixture.
Why 4
Why 5
Root Cause (Occurance) Fixture Clamping Loose from one side.
 
Root Cause Analysis (Outflow)
Why 1 100 % inspection at final stage without marking.
Why 2 Operator knowledge not found evident.
Why 3
Why 4
Why 5
Root Cause (Outflow) 100 % Inspection at Final stage without marking
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceProper Tight Clamping Fixture Both side.Mr. Thakur.23/03/202223/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Start 100% inspection with identification marking.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Fixture PM check sheet.
73_Occurance_Before.xlsx
Occurance (After) Fixture PM check sheet & JH check sheet
73_Occurance_After.xlsx
Outflow (Before) Without marking.
73_Outflow_Before.jpg
Outflow (After) Inspection marking.
73_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Not applicable
 
12. Document Review
Documents PMCheckSheet, JHCheckSheet, InspCheckSheet
Specify Other Document Fixture check sheet.
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission OK