QFR No - 7000834209
Defect Details
NC No. 7000834209
NC Date 30/04/2022
NC Submission Date
Part No. 520FN01902
Part Name CLUTCH HOLDER BM-150
Supplier Name & Code 202375-ADVANTECH ENGINEERING COMPANY
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DIMETER UNDERSIZE-4Hole Dia 6.2+01 o/s no go Gauge Qualyfn
 
1. Problem Description
Defect Description 4 Hole Dia 6.2+01 oversize no go Gauge Qualifying
Detection Stage Receipt
Problem Severity Function
NG Quantity 320
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@advantechgroup.co.in
Plant Head/CEO Email ID info@advantechgroup.co.in
MD Email ID harishpathade@advantechgroup.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1200
0
0
1500
800
3500
Check Qty
1200
0
0
1500
800
3500
NG Qty
320
0
0
0
0
320
 
Scrap 320
Rework 0
Under Deviation 0
Containment Action
On VMC PCD Hole Carbide step drill (size 6.28 mm) replaced and new size of drill 6.24 mm for maintain hole ID 6.2+0.1 mm. Drill change frequency after 40000 nos.
 
3. Process Flow
Process Flow Description
Receiving of Casting + CNC Turning -- VMC 4 hole drilling --- Final inspection --Dispatch
 
4. Process Details
Process / Operation CNC- Turning, VMC- PCD hole Drill
Outsource No
Machine / Cell Machine Shop
Machine / Cell No. VMC - 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachinePCD hole ID 6.2+0.1 mm taken higher side.No Go passO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 32
7. Root Cause Analysis (Occurance)
Why 1 PCD Hole ID 6.2+0.1 mm No GO Passed
Why 2 PCD hole ID 6.2 +0.1 taken higher side as per customer requirement.
Why 3 PCD hole step drill size 6.28 mm
Why 4
Why 5
Root Cause (Occurance) On VMC PCD hole step drill size 6.28 mm
 
Root Cause Analysis (Outflow)
Why 1 PCD Hole ID 6.2+0.1 mm No GO Passed
Why 2 PCD hole ID - inspection not done with plug gauge at final stage.
Why 3 PCD hole ID by Plug gauge - I Do I check by operator at Machining stage.
Why 4
Why 5
Root Cause (Outflow) PCD hole ID by Plug gauge - I Do I check by operator at Machining stage.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. On VMC PCD hole step drill size 6.28 mm replaced with new size 6.24 mm 2. Hole ID inspection started by Plug gauge at final stage on sampling basis.Mr. Kuldeep /Vasant03/05/202203/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Hole ID inspection started by Plug gauge at final stage on sampling basis.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
10. Evidance of Countermeasure
Occurance (Before) PCD Hole Step Drill Size-6.28 mm
83_Occurance_Before.xlsx
Occurance (After) PCD Hole Step Drill Size-6.24 mm
83_Occurance_After.xlsx
Outflow (Before) Plug Gauge inspection at VMC machine after hole drill operation
83_Outflow_Before.xlsx
Outflow (After) Plug gauge inspection started at final stage as per sampling plan
83_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, WISOP, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission Cause side and inspection side action not proper