QFR No - 7000836634
Defect Details
NC No. 7000836634
NC Date 17/05/2022
NC Submission Date
Part No. F2LY00312B
Part Name SOCKET HEADED BOLT M8 - PRECOTE
Supplier Name & Code 100348-SINGLA FORGING
ETL Plant 1126-ETL Pantnagar
Defect Details LEAKAGE-
 
1. Problem Description
Defect Description Uneven face/cut marks of Copper Washer resting area in Socket Head Bolt (F2LY00312B).
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1701
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pntquality@singlaforging.in
Plant Head/CEO Email ID deepakgupta@singlaforging.com
MD Email ID jain@singlaforging.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
17000
0
0
5000
12000
34000
Check Qty
17000
0
0
5000
12000
34000
NG Qty
1701
0
0
86
47
1834
 
Scrap 1834
Rework 0
Under Deviation 0
Containment Action
1-100% segregation of material lying at various stages is started with OK confirmation marking. 2- Quality Alert to be displayed at the work station.
 
3. Process Flow
Process Flow Description
Operation /No Operation:- 10 -Receipt of Material , 20- Forging, 30- Thread Rolling, 40- Heat Treatment, 50- Packaging and dispatch, 60-Receipt of forging, 70-incoming inspection, 80-Storage, 90-Surface treatment,100-Final Inspection,110-Packaging,120-Dispatch
 
4. Process Details
Process / Operation Forging
Outsource Yes
Machine / Cell Forging
Machine / Cell No. Forging
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWrong materialRaw Material used as per drawing with all Quality Parameters CheckedO
ManUnskilled & unawareInspector was not detect defective part as the part is in Black Condition so it was difficult to ObsO
MethodInspection frequency not adequateChecked and verfiied ispection frequecy followed as per control plan 05 Pcs per HourO
MethodNG part mix woth ok partSaperate location for OK and NG part, Red Bins Provided @ Forging StageO
MachineTool life not followChecked and verified tool life monitored and followed but Need to be Validated as Complaint is raisX
MachineSetup errorchecked and verified setting procedure followed for settingO
MachineDie Crack markCheck and found that die got cracked in running productionX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Samp. Plan
7. Root Cause Analysis (Occurance)
Why 1 The Problem Occurred @Cold Forging Stage of the manufacturing Sequence
Why 2 Here Hex Socket ,Head Dia & Head Height are Formed in One Die
Why 3 Due to the nature of the process There is a Heavy Load in Die So Chances are More for Die to get Wear
Why 4 `Due to This Wear A Fine Line mark Was Created @ Bearing face
Why 5 This Fine Line mark was difficult to identify in Black Condition during WIP Stage
Root Cause (Occurance) Die got cracked in running production due to high load on-die during making the socket and head in one Die.
 
Root Cause Analysis (Outflow)
Why 1 Defected Part not detected in final inspection stage
Why 2 Inspection was as per sampling Plan.
Why 3 This Fine Line mark was difficult to identify in Black Condition during WIP Stage
Why 4
Why 5
Root Cause (Outflow) This Fine Line mark was difficult to identify as the part is in Black Condition during WIP Stages before Plating. After Plating Such Defects get Clearly Visible
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance2-OJT training to be provided to the operator to Understand the Problem, Its Impact & Countermeasures..Nishant01/07/202201/07/2022Completed
Outflow1-Quality Alert is displayed in final inspection stageNishant17/05/202217/05/2022Completed
Outflow2-Awareness training to be provided to the inspector to Understand the Problem, Its Impact & Countermeasures.Nishant16/05/202217/05/2022Completed
Occurance1- Part M8X27 Head Forging Die`s Scheduled Maintenance to be Done At Forging of 1 Lacs Pcs with Light Polishing & Same will be Recorded in Die History cardNishant Jangra01/07/202201/07/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Part M8X27 Head Forging Die`s Scheduled Maintenance to be Done At Forging of 1 Lacs Pcs with Light Polishing & Same will be Recorded in Die History card
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Quality alert to be displayed
121_Occurance_Before.pdf
Occurance (After) 1- Part M8X27 Head Forging Die`s Scheduled Maintenance to be Done At Forging of 1 Lacs Pcs with Light Polishing & Same will be Recorded in Die History card 2-OJT training to be provided to the operator to Understand the Problem, Its Impact & Countermeasures..
121_Occurance_After.pdf
Outflow (Before) Visual inspection done with naked eye
121_Outflow_Before.xlsx
Outflow (After) 1-Quality Alert is displayed in final inspection stage 2-Awareness training to be provided to the inspector to Understand the Problem, Its Impact & Countermeasures.
121_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Bolt
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document OJT
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission found OK