QFR No - 7000838557
Defect Details
NC No. 7000838557
NC Date 25/05/2022
NC Submission Date
Part No. S2HT52107B
Part Name OUTER SPRING K0PG
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details NOT AS PER SPECIFICATION-Grinding Angle Less than 270 °
 
1. Problem Description
Defect Description Grinding angel found less i.e. observed 190, 185, 220 degree against the spec of 270 degree min.
Detection Stage Receipt
Problem Severity Function
NG Quantity 1820
Is Defect Repeatative? No
Defect Sketch / Photo 3jd0wsglcjllsqocql1hxmsz.jpg
Supplier Communication Details
Quality Head Email ID ravindra@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1820
0
0
0
4000
5820
Check Qty
1820
0
0
0
4000
5820
NG Qty
1820
0
0
0
0
1820
 
Scrap 0
Rework 0
Under Deviation 1820
Containment Action
Check all material found ok at helical end found ok.
 
3. Process Flow
Process Flow Description
RM>Coiling> SR1>Grinding>Shot peening >Correction>Powder Coating>PDI>Packing> Dispatch.
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell Grinding M/c
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Machinenot feasible to maintaingrinding angle 250 degO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 nos
7. Root Cause Analysis (Occurance)
Why 1 Grinding angle less observed
Why 2 grinding angle not achieved in grinding
Why 3 due to length variation, the grinding angle less
Why 4 grinding angle required is 250 deg min
Why 5 --
Root Cause (Occurance) grinding angle required is 250 deg min
 
Root Cause Analysis (Outflow)
Why 1 Grinding angle less observed
Why 2 Not arrested in existing sampling due to less in no.
Why 3 --
Why 4 --
Why 5 --
Root Cause (Outflow) Not arrested in existing sampling due to less in no.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDrawing modified and updated for Grinding angleETL-HELICAL30/05/202208/08/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No change
Inspection Method Other
Other Inspection Method visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 nos
10. Evidance of Countermeasure
Occurance (Before) Drawing with grinding angle 270 deg min
151_Occurance_Before.pdf
Occurance (After) Drawing with grinding angle 250 deg min
151_Occurance_After.pdf
Outflow (Before) Acceptance criteria - 270 deg min
151_Outflow_Before.pdf
Outflow (After) Acceptance criteria - 250 deg min
151_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant no
 
12. Document Review
Documents Drawing, ControlPlan, WISOP, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 0
Reason for submission Grinding leas