QFR No - 7000838557
Defect Details
NC No. | 7000838557 |
NC Date | 25/05/2022 |
NC Submission Date | |
Part No. | S2HT52107B |
Part Name | OUTER SPRING K0PG |
Supplier Name & Code | 101225-HELICAL SPRINGS |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | NOT AS PER SPECIFICATION-Grinding Angle Less than 270 ° |
1. Problem Description
Defect Description | Grinding angel found less i.e. observed 190, 185, 220 degree against the spec of 270 degree min. |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 1820 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | 3jd0wsglcjllsqocql1hxmsz.jpg |
Supplier Communication Details
Quality Head Email ID | ravindra@helicalsprings.in |
Plant Head/CEO Email ID | shaikhmoin@helicalsprings.in |
MD Email ID | ataneja@helicalsprings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1820
|
0
|
0
|
0
|
4000
|
5820
|
Check Qty |
1820
|
0
|
0
|
0
|
4000
|
5820
|
NG Qty |
1820
|
0
|
0
|
0
|
0
|
1820
|
Scrap | 0 |
Rework | 0 |
Under Deviation | 1820 |
Containment Action |
---|
Check all material found ok at helical end found ok. |
3. Process Flow
Process Flow Description |
---|
RM>Coiling> SR1>Grinding>Shot peening >Correction>Powder Coating>PDI>Packing> Dispatch. |
4. Process Details
Process / Operation | Grinding |
Outsource | No |
Machine / Cell | Grinding M/c |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | not feasible to maintain | grinding angle 250 deg | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Grinding angle less observed |
Why 2 | grinding angle not achieved in grinding |
Why 3 | due to length variation, the grinding angle less |
Why 4 | grinding angle required is 250 deg min |
Why 5 | -- |
Root Cause (Occurance) | grinding angle required is 250 deg min |
Root Cause Analysis (Outflow)
Why 1 | Grinding angle less observed |
Why 2 | Not arrested in existing sampling due to less in no. |
Why 3 | -- |
Why 4 | -- |
Why 5 | -- |
Root Cause (Outflow) | Not arrested in existing sampling due to less in no. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Drawing modified and updated for Grinding angle | ETL-HELICAL | 30/05/2022 | 08/08/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No change |
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 nos |
10. Evidance of Countermeasure
Occurance (Before) |
Drawing with grinding angle 270 deg min 151_Occurance_Before.pdf |
Occurance (After) |
Drawing with grinding angle 250 deg min 151_Occurance_After.pdf |
Outflow (Before) |
Acceptance criteria - 270 deg min 151_Outflow_Before.pdf |
Outflow (After) |
Acceptance criteria - 250 deg min 151_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | no |
12. Document Review
Documents | Drawing, ControlPlan, WISOP, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 0 |
Reason for submission | Grinding leas |