QFR No - 7000838558
Defect Details
NC No. 7000838558
NC Date 25/05/2022
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details PARALITY NOT OK.-Perpendicularity Out of Spec
 
1. Problem Description
Defect Description Perpendicular NG i.e. observed 1.44, 1.37, 0.85 mm against the spec of 0.5 mm Max.
Detection Stage Receipt
Problem Severity Function
NG Quantity 3400
Is Defect Repeatative? Yes
Defect Sketch / Photo 3jd0wsglcjllsqocql1hxmsz.jpg
Supplier Communication Details
Quality Head Email ID ravindra@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15400
0
0
0
8450
23850
Check Qty
15400
0
0
0
8450
23850
NG Qty
15400
0
0
0
0
15400
 
Scrap 0
Rework 0
Under Deviation 15400
Containment Action
All material used under deviation. we maintain e2 within spec 1.00 mm Max.
 
3. Process Flow
Process Flow Description
RM>Coiling>SR1>Grinding>Shotpeening>Setting>Correction>SR2>PDI>Packing>Dispatch.
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell Grinding
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine check Sheet not followedCLIT verified found okO
Methodtop and bottom grinding plate hole alignment not okAlignment found disturbX
Manunskilled OperatorSkill matrix checked found okO
MaterialAs per Drawing Not okRMTC verified found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 29/3201
7. Root Cause Analysis (Occurance)
Why 1 Perpendicularity Observed 0.7MM Against 0.5MM Max.
Why 2 Due to taper grinding.
Why 3 Top grinding plate position disturb w .r. t. bottom grinding plate
Why 4 Single nut locking system available
Why 5
Root Cause (Occurance) Single nut locking system available
 
Root Cause Analysis (Outflow)
Why 1 Perpendicularity Observed 0.7MM Against 0.5MM Max
Why 2 No inspection for e2
Why 3 No check point in line inspection for e2
Why 4
Why 5
Root Cause (Outflow) No check point in line inspection for e2
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAdditional locking pins provided into both plates to fix the position.Mr. Niesh Kapure22/02/202221/02/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Introduced the perpendicularity in line inspection
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 23/3200
10. Evidance of Countermeasure
Occurance (Before) Single nut locking system available
150_Occurance_Before.jpg
Occurance (After) Additional locking pins provided into both plates to fix the position
150_Occurance_After.jpg
Outflow (Before) No check point in line inspection for e2
150_Outflow_Before.pdf
Outflow (After) Introduced the perpendicularity in line inspection
150_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All main Spring
 
12. Document Review
Documents InspCheckSheet
Specify Other Document Patrolling Insp
 
13. Effectiveness Of Action
Reviewed Quantity 0
Reason for submission ok