QFR No - 7000838558
Defect Details
NC No. | 7000838558 |
NC Date | 25/05/2022 |
NC Submission Date | |
Part No. | F1GN01102B |
Part Name | MAIN SPRING K86A |
Supplier Name & Code | 101225-HELICAL SPRINGS |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | PARALITY NOT OK.-Perpendicularity Out of Spec |
1. Problem Description
Defect Description | Perpendicular NG i.e. observed 1.44, 1.37, 0.85 mm against the spec of 0.5 mm Max. |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 3400 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 3jd0wsglcjllsqocql1hxmsz.jpg |
Supplier Communication Details
Quality Head Email ID | ravindra@helicalsprings.in |
Plant Head/CEO Email ID | shaikhmoin@helicalsprings.in |
MD Email ID | ataneja@helicalsprings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
15400
|
0
|
0
|
0
|
8450
|
23850
|
Check Qty |
15400
|
0
|
0
|
0
|
8450
|
23850
|
NG Qty |
15400
|
0
|
0
|
0
|
0
|
15400
|
Scrap | 0 |
Rework | 0 |
Under Deviation | 15400 |
Containment Action |
---|
All material used under deviation. we maintain e2 within spec 1.00 mm Max. |
3. Process Flow
Process Flow Description |
---|
RM>Coiling>SR1>Grinding>Shotpeening>Setting>Correction>SR2>PDI>Packing>Dispatch. |
4. Process Details
Process / Operation | Grinding |
Outsource | No |
Machine / Cell | Grinding |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Machine check Sheet not followed | CLIT verified found ok | O |
Method | top and bottom grinding plate hole alignment not ok | Alignment found disturb | X |
Man | unskilled Operator | Skill matrix checked found ok | O |
Material | As per Drawing Not ok | RMTC verified found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 29/3201 |
7. Root Cause Analysis (Occurance)
Why 1 | Perpendicularity Observed 0.7MM Against 0.5MM Max. |
Why 2 | Due to taper grinding. |
Why 3 | Top grinding plate position disturb w .r. t. bottom grinding plate |
Why 4 | Single nut locking system available |
Why 5 | |
Root Cause (Occurance) | Single nut locking system available |
Root Cause Analysis (Outflow)
Why 1 | Perpendicularity Observed 0.7MM Against 0.5MM Max |
Why 2 | No inspection for e2 |
Why 3 | No check point in line inspection for e2 |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No check point in line inspection for e2 |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Additional locking pins provided into both plates to fix the position. | Mr. Niesh Kapure | 22/02/2022 | 21/02/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Introduced the perpendicularity in line inspection |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 23/3200 |
10. Evidance of Countermeasure
Occurance (Before) |
Single nut locking system available 150_Occurance_Before.jpg |
Occurance (After) |
Additional locking pins provided into both plates to fix the position 150_Occurance_After.jpg |
Outflow (Before) |
No check point in line inspection for e2 150_Outflow_Before.pdf |
Outflow (After) |
Introduced the perpendicularity in line inspection 150_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All main Spring |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | Patrolling Insp |
13. Effectiveness Of Action
Reviewed Quantity | 0 |
Reason for submission | ok |