QFR No - 7000842723
Defect Details
NC No. | 7000842723 |
NC Date | 17/06/2022 |
NC Submission Date | |
Part No. | 53BHT00807 |
Part Name | OUTER SPRING POWDER COATED-VAVE |
Supplier Name & Code | 101048-STUMPP SCHUELE AND SOMAPPA SPR |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | POWDER COATING NOT OK-Powder coating Defects . |
1. Problem Description
Defect Description | Powder coating Defects like White Spot, Heavy Hanger Marke, Pin Hole, Paint Uncover & Dry etc. |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 271 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | vipin.shukla@ssssprings.com |
Plant Head/CEO Email ID | udham.singh@ssssprings.com |
MD Email ID | rln@ssssprings.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1120
|
0
|
0
|
1120
|
0
|
2240
|
Check Qty |
1120
|
0
|
0
|
1120
|
0
|
2240
|
NG Qty |
8
|
0
|
0
|
0
|
0
|
8
|
Scrap | 8 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Visual Inspection |
3. Process Flow
Process Flow Description |
---|
Recipt & inspection - Storage of material - Winding - Stress Relieving-1 - Grinding - Shot peening - Stress Releiving-2 - Scragging - Length,e1,e2 sorting - powder coating - Final inspection - Packing |
4. Process Details
Process / Operation | Powder Coating |
Outsource | No |
Machine / Cell | PC Line |
Machine / Cell No. | Powder Coating |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | improper handling of the parts | Verified and found that parts fall down during hanging process and got dust accumulated | X |
Method | OK and NG parts mix up during inspeciton | Inspected OK parts and Parts pending for inspection got mix up | X |
Material | parts not cleaned during PT process | Process verified and found satisfactory PT process | O |
Man | Unskilled person deputed for powder coated springs | Verified the skill level of the inspector and found OK | O |
Machine | Powder coating gun parameters not as per specification | Verified all the machine parameters & found within specification | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Problem occured during powder coating process. |
Why 2 | Dust accumulation during process |
Why 3 | Few parts dropped down while loading/hanging to hangers & loaded again without cleaning. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Few parts dropped down while loading/hanging to hangers & loaded again without cleaning. |
Root Cause Analysis (Outflow)
Why 1 | Defective part escaped through inspection |
Why 2 | NG parts mixed up with OK parts. |
Why 3 | Inspected OK parts and parts pending for inspection got mix up |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspected OK parts and parts pending for inspection got mix up |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Design of the hangers modified to avoid the fall of spring during hanging process | Mr Shashank | 23/06/2022 | Pending | |
Outflow | Separator provided at inspection table to avoid the mix up of "Inspection finished parts" and "parts pending for inspection" | Mr. Shashank | 22/06/2022 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Separator provided at inspection table to avoid the mix up of "Inspection finished parts" and "parts pending for inspection |
Inspection Method | Pokayoke |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No work instruction found for the treatment of fallen parts during hanging of springs during powder coating process 181_Occurance_Before.pdf |
Occurance (After) |
Work instruction revised for the instructions on treatment of fallen parts 181_Occurance_After.pdf |
Outflow (Before) |
Inspection finished parts and Inspection pending parts were kept together without separator. 181_Outflow_Before.png |
Outflow (After) |
Separator provided to avoid accumulation at inspection table for the isnpected parts and inspection pending parts 181_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Horizontal deployment for Occurrence and Outflow actions for all OC springs |
12. Document Review
Documents | WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |