QFR No - 7000849927
Defect Details
NC No. 7000849927
NC Date 19/07/2022
NC Submission Date
Part No. 530DC00802
Part Name INNER DUST COVER
Supplier Name & Code 101135-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1136-ETL Suspension Sanand
Defect Details NOT AS PER LIMIT SAMPLE- Rubbing mark,scratch mark,visual Defect
 
1. Problem Description
Defect Description Dent & Scratches
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 3537
Is Defect Repeatative? No
Defect Sketch / Photo djmfyappvchnnfd1btqarm1q.jpg
Supplier Communication Details
Quality Head Email ID qms@jairajgroup.com
Plant Head/CEO Email ID agm.sanand@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
8500
0
0
2000
0
10500
Check Qty
8500
0
0
2000
0
10500
NG Qty
6910
0
0
235
0
7145
 
Scrap 235
Rework 0
Under Deviation 0
Containment Action
1. 100 % inspection done at ETL end & checked all the material from all stages. 2. Defective parts from WIP & FG stock are scrapped - Total scrap qty - 235 no`s , Dated on 21.07.2022
 
3. Process Flow
Process Flow Description
RM Receiving - Inward Inspection - RM issue to Production - Injection Molding Process - Degating/Deflashing - Final Inspection - Packing & Identification -PDI - Dispatch
 
4. Process Details
Process / Operation Injection molding
Outsource No
Machine / Cell IMM
Machine / Cell No. IMM-07/E140T
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodProcess Parameter Not follow as per OCS/CPVerifi ed Process parameter as per Control plan found OKO
MachineMachine changeVerified the mold machine matrix & found ok . Parts produced on defined machine as per matrixO
ManUnskilled Operator or Inspector Awareness about the defectShill evaluation done about the defect awareness - found okO
MaterialRM Grade not as per specificationSupplier RMTC Verified and Third party Testing done from NABL approved lab for PPCP RM.O
ToolTool Preventive Maintenance not done as per schedule.Verified Tool PM schedule with actual PM- Found OK . Tool surface gloss found dullX
MethodMaterial handling method is inappropriateVerified handling method. Improvement required to avoid direct contact of parts with plastic binX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size -
7. Root Cause Analysis (Occurance)
Why 1 Method of handling is inappropriate at several stages for glossy parts resulting into visual defects
Why 2 Less awareness about material handling for glossy parts as there is Direct contact of parts with plastic bin
Why 3
Why 4
Why 5
Root Cause (Occurance) Less awareness about material handling for glossy parts
 
Root Cause Analysis (Outflow)
Why 1 Defective parts skipped to customer
Why 2 Defect is not detected at final inspection stage
Why 3 Material handling after final inspection done inappropriate way resulting into visual defects
Why 4
Why 5
Root Cause (Outflow) Material handling after final inspection done inappropriate way resulting into visual defects
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool PM frequency to be verified and cavity gloss verification term added in PM Check sheet.Mr.Nilesh Patil22/07/202222/07/2022Completed
OutflowOPL & Q Alert to be Displayed at defect occurrence stageMr. Sachin Kulkarni22/07/202222/07/2022Completed
OccuranceImplement packing standard wrt material handling to avoid direct contact of parts with plastic binMr. Sachin Kulkarni22/07/202222/07/2022Completed
OutflowOn Job Training to be given to concerned peoplesMr. Sachin Kulkarni23/07/202223/07/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details -
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size -
10. Evidance of Countermeasure
Occurance (Before) Material handling done in plastic bin
207_Occurance_Before.pdf
Occurance (After) Material handling improved as polybag implemented on machine . No use of plastic bin to avoid direct contact of parts with bin
207_Occurance_After.pdf
Outflow (Before) At final inspection stage, packing is inappropriate resulting visual defects as packing & dispatch activity to be carried out after this.
207_Outflow_Before.pdf
Outflow (After) Packing standard implemented at final inspection stage . After inspection , standard size of 100 no`s will be packed in stacking order with polybag.
207_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant -
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA, WISOP, PackingStd, InspCheckSheet
Specify Other Document -
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission Verified improve lot and found effective. Also verified minor correction in arranging of material in packing improved material condition.