QFR No - 7000852947
Defect Details
NC No. 7000852947
NC Date 01/08/2022
NC Submission Date
Part No. 520AE04002
Part Name CORE PLATE (C20002)
Supplier Name & Code 100915-CHIRAG DIE CAST PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details NOT AS PER SPECIFICATION-hardness obs 37 ~46 hrb against 52~62 hr
 
1. Problem Description
Defect Description Hardness Observed 37 ~46 HRB As against 52~62 HRB
Detection Stage Receipt
Problem Severity Function
NG Quantity 1000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityassurance@chiragdiecast.com
Plant Head/CEO Email ID operationshead@chiragdiecast.com
MD Email ID chirag.gupta@chiragdiecast.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
0
0
1000
Check Qty
1000
0
0
0
0
1000
NG Qty
1000
0
0
0
0
1000
 
Scrap 1000
Rework 0
Under Deviation 0
Containment Action
Tested samples will be send with each lot for Cross Verification
 
3. Process Flow
Process Flow Description
PDC , Trimming & shaving , Shot Blasting , Visual Inspection , Stress Reliving, 100% Gauging for Flatness, Packing & Dispatch
 
4. Process Details
Process / Operation High Pressure Die Casting
Outsource No
Machine / Cell HPDC
Machine / Cell No. PDC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialMg. at Lower side of Specification of ADC-12Mg. observed in component 0.18O
MethodMeasurement Variation in Hardness TestingDifference observed upto 6 points in HRBO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5 pcs .
7. Root Cause Analysis (Occurance)
Why 1 Mg. found lower side 0.12% as against 0.30 Max. specification of ADC-12
Why 2 Mg. burn during HPDC process
Why 3 Symptoms / phenomenon of process
Why 4
Why 5
Root Cause (Occurance) Lower side Mg.% will affect the hardness in lower side against the specification.
 
Root Cause Analysis (Outflow)
Why 1 Part to part & Claw to claw variation ( In our samples we have observed 48 to 58 HRB
Why 2 Mix up of Runner riser in PDC Process ( 2 or 3 Times)
Why 3 Mixing of Runner Riser & al. Ingot is the part of process.
Why 4
Why 5
Root Cause (Outflow) Hardness Tester results variation & Mg % Variation Part to Part & Claw to claw variation.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowWe will send 5 Pcs duly hardness tested with each lot for cross verification.Chirag Die Cast18/08/202218/08/2022Completed
OccuranceWe will maintain % age of Mg. in molten Material Minimum 0.20% by addition of Pure Mg. ( On the basis of as & when required) during PDC process.Chirag Die Cast18/08/202218/08/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 Nos.
10. Evidance of Countermeasure
Occurance (Before) We were not adding Mg. during HPDC Process
217_Occurance_Before.pdf
Occurance (After) As per Process Inspection Report PDC , we have maintain the % of Mg as Min 0.2% in Molten Material & Hardness observed ( 48 to 60 HRB )
217_Occurance_After.pdf
Outflow (Before) No submission of hardness tested samples for cross verification
217_Outflow_Before.pdf
Outflow (After) We will send 5 Pcs. duly hardness tested with each lot for cross verification at ETL to ensure variation in Testing Machine.( 10 Points band of Hardness requesting to increase ) as same Pc covered all the tolerance band.
217_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for other core plates , where ETL asked for Hardness .
 
12. Document Review
Documents WISOP
Specify Other Document PIR for Mg add & HRB
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission OK