QFR No - 7000869422
Defect Details
NC No. 7000869422
NC Date 10/10/2022
NC Submission Date
Part No. 520GR00102
Part Name MEMBRANE
Supplier Name & Code 203807-ROOP POLYMERS LTD.
ETL Plant 1126-ETL Pantnagar
Defect Details LEAKAGE-Leakage Due to non-filling
 
1. Problem Description
Defect Description Leakage issue due to Non Filling at O Ring
Detection Stage Receipt
Problem Severity Function
NG Quantity 9000
Is Defect Repeatative? Yes
Defect Sketch / Photo cwg20gmhnzlfu0ffjmtswljj.jpg
Supplier Communication Details
Quality Head Email ID prem.singh@rooppolymers.com
Plant Head/CEO Email ID ashish.grover@rooppolymers.com
MD Email ID pbs.rawat@rooppolymers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
500
200
2700
Check Qty
2000
0
0
500
200
2700
NG Qty
12
0
0
5
0
17
 
Scrap 10
Rework 7
Under Deviation 0
Containment Action
Verify the available lot @ ETL as well as plant
 
3. Process Flow
Process Flow Description
Rubber Molding.
 
4. Process Details
Process / Operation Molding
Outsource No
Machine / Cell 08
Machine / Cell No. 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodMaterial Loading Pattern Not Followed.Found As per PCS.O
ManLess skilled operatorSkilled level 3 operator , as per skill matrixO
MachineLevel of Machine Not OKLevel found within 0.025mm against spec 0.5mmO
MaterialHardness of Material ExcessFound 55 Shore AO
ToolLeakage From Pocket & PlungerGap Observed in Plunger & Pocket.X
ManLess input weight placed by operatorChecked weight & found OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Leakage issue due to Non Filling at O Ring area
Why 2 Material Leakage from Transfer Pocket
Why 3 Clearance observed in Pocket & Plunger corners.
Why 4
Why 5
Root Cause (Occurance) Clearance observed in Pocket & Plunger corners.
 
Root Cause Analysis (Outflow)
Why 1 Non filling @ O- ring Out flowed to customer.
Why 2 Defective Part Mix-up with OK Parts
Why 3 Small Red Bin Installed @ top of Inspection Table.
Why 4
Why 5
Root Cause (Outflow) Small Red Bin Installed @ top of Inspection Table.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePocket & Plunger welding & matching done to prevent LeakageDaler Singh14/10/202214/10/2022Completed
OutflowTraining given to concerned InspectorRishabh Rastogi14/10/202214/10/2022Completed
OutflowRed Bin Location Defined inside the Inspection table & Hole Given on top of the table to place the part into red bin.Rishabh Rastogi13/10/202214/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details 100% Visual Inspection available.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Clearance between Plunger & Pocket.
280_Occurance_Before.jpg
Occurance (After) Welding & Matching done on plunger to prevent Leakage
280_Occurance_After.jpg
Outflow (Before) Red Bin is above the table, NG Part Mixed with OK Parts.
280_Outflow_Before.jpg
Outflow (After) Red Bin placed Under rack, Hole Given for Part placing into red bin.
280_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Rubber Moulding
 
12. Document Review
Documents WISOP
Specify Other Document Tool History Card
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission Found OK