QFR No - 7000870350
Defect Details
NC No. 7000870350
NC Date 12/10/2022
NC Submission Date
Part No. S2HT12007B
Part Name INNER SPRING_B104_E
Supplier Name & Code 100834-LALJI GOPINATHJI INDUSTRIES
ETL Plant 1126-ETL Pantnagar
Defect Details DIAMETER OVER SIZE-I/D Undersize in Inner Spring B104E
 
1. Problem Description
Defect Description I/D Undersize in Inner Spring B104E (S2HT12007B).
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 238
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID std@lgindustries.co.in
Plant Head/CEO Email ID rahulkumar@lgindustries.co.in
MD Email ID lalit.k@lgindustries.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2968
0
0
1000
0
3968
Check Qty
2968
0
0
1000
0
3968
NG Qty
238
0
0
0
0
238
 
Scrap 238
Rework 0
Under Deviation 0
Containment Action
1-Immediate supply stopped only for next lot to verify the problem at our end.,2-All the pipeline parts seggrigated and NG parts removed from the shop flore.and.Only 100 % inspected material should be supplied to customer.
 
3. Process Flow
Process Flow Description
1.Incoming Rm ,2- coiling .3-Tempring,4-greanding .5-shoot peening ,6-Recovery,7-secend Tempring ,8-powder caoting,9-PDI inspection ,10-Dispatch
 
4. Process Details
Process / Operation PDI Stage
Outsource No
Machine / Cell CNC coiling m/c
Machine / Cell No. CSK-690
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolGaugeTo be verified in internal calibration std room by Micrometer found whithin spcifactionO
Machinecoiling m/cTo be verified all cnc process parameter found ok within specificationO
MethodInspectionDue to not proper checking inspection as par frequencyX
ManNegligence of PDI inspectorPDI Inspector Negligence that they not do proper checked 100%X
MaterialRMTo be verified as par incoming inspection check sheet&With TC Found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 0
7. Root Cause Analysis (Occurance)
Why 1 spring inner diameter under size
Why 2 spring inner diameter under size found after Powder coating
Why 3 spring inner Diameter Found lower side during coiling Lower side (29.9mm)
Why 4
Why 5
Root Cause (Occurance) spring inner diameter found Lower side specification (29.90 mm-30.30mm)
 
Root Cause Analysis (Outflow)
Why 1 spring inner diameter Found undersize
Why 2 after powder coating 100 % inspection not proper done by PDI inspector
Why 3 lack of Awareness of PDI about spring ID Fitment
Why 4
Why 5
Root Cause (Outflow) Due to PDI inspector negligence that they not do proper CHECKD by gauge
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowOperator`s on the job training done shox assembly fitment parameter and OPL Display for fitment parameter on powder coating both ,and 100 % inspection to be verified on the PDI stage by QA inspector sampling basisMr.umesh tiwari and Sunil18/10/202218/10/2022Completed
OccuranceTo maintain inner Diameter higher side within specification (30.10-30.30mm)MR.Sunil18/10/202218/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details we have already 100% checked by PDI inspector But crossed verified after PDI stage checked sampling basis by QA
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size sam.plan
10. Evidance of Countermeasure
Occurance (Before) Before powder coating we have used this inner id gauge within specification (29.25-29.90 mm)
283_Occurance_Before.jpg
Occurance (After) To be interduce new gauge for before powder coating stage and specification within (30.00-30.30)
283_Occurance_After.jpg
Outflow (Before) operator not proper aware for shox assembly fitment at the PDI Stage, no sampling plan after inspection
283_Outflow_Before.pdf
Outflow (After) 1-Proper training is given to PDI inspector for inner dia fitment issue ,2-Samplening plan is made for after final inspection ,3-WI/OPL Displayed for 100% inner dia inspection at relevent stage
283_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant spring division
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission Found OK