QFR No - 7000870351
Defect Details
NC No. 7000870351
NC Date 12/10/2022
NC Submission Date
Part No. 520JF00123
Part Name PISTON GROOVED
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1126-ETL Pantnagar
Defect Details RUSTY-Rusty
 
1. Problem Description
Defect Description Rusty
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 1614
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Rajendra.Sethiya@gknpm.com
Plant Head/CEO Email ID Pratik.Dharangaonkar@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
24000
0
0
40000
38000
102000
Check Qty
24000
0
0
40000
38000
102000
NG Qty
1696
0
0
0
0
1696
 
Scrap 1696
Rework 0
Under Deviation 0
Containment Action
All stock lying at ETL segregated for rusty issue, GKN FG stock quarantined & verified. Quality Alert raised at Tier 1 & Final inspection
 
3. Process Flow
Process Flow Description
Forming - Sintering - Sizing -Machining - Oil dipping -Packing - PDI Inspection
 
4. Process Details
Process / Operation Machining
Outsource Yes
Machine / Cell Oil dipping
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodDewatering NGGemba conducted with CGT at Supplier End observed excess qty loaded for dewateringX
MaterialParts Metallurgy NGParts are OK to the metallurgical check and found okO
ManSkipped in inprocess and Final inspectionDuring inprocess inspection parts was rust free but possibility to rust furtherO
ManUntrained OperatorOperator skill matrix is okO
MethodWrong DW oil grade usedDewatering Oil grade DW27 is found with correct grdaeO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
7. Root Cause Analysis (Occurance)
Why 1 Parts are not completely dipped into dewatering tank
Why 2 Excess part quantity taken for Oil dipping
Why 3 Parts in tray carrying for dewatering is taken more
Why 4 As per daily schedule of production, less capacity of dewatering
Why 5 Only single dewatering tank was available
Root Cause (Occurance) Excess part quantity taken for Oil dipping
 
Root Cause Analysis (Outflow)
Why 1 Skipped in in process and Final inspection
Why 2 Parts was found ok during inspection
Why 3 Parts was rust free after final inspection
Why 4 After final inspection , parts was ok at GKN pdi
Why 5 Parts gets rusty after clearing the material from PDI
Root Cause (Outflow) Parts gets rusty after clearing the material from PDI
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1.Oil dipping tanks will be marked with red , yellow and green oil leval.B Avhad06/01/2023Completed
OccuranceRefreshment training is provided to all operators and inspectors thru One Point lesson and quality alert.B Avhad16/12/2022Completed
OccuranceAddiitional one Dewatering Tank will be made availableB Avhad07/12/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NA
Inspection Method Other
Other Inspection Method NA
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 0
10. Evidance of Countermeasure
Occurance (Before) No Marking/Identification on Oil Tank
284_Occurance_Before.pdf
Occurance (After) Oil dipping tanks will be marked with red , yellow and green oil level.
284_Occurance_After.pdf
Outflow (Before) NA
284_Outflow_Before.pdf
Outflow (After) NA
284_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission Found OK