QFR No - 7000876117
Defect Details
NC No. 7000876117
NC Date 11/11/2022
NC Submission Date
Part No. 520AE05702
Part Name CORE PLATE - SHINE & UNICORN
Supplier Name & Code 101145-STAR PROJECTS INDIA
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details FLATNESS NOT OK.-Ga gauge not qualify due to flatness o/s
 
1. Problem Description
Defect Description Flatness Not OK -Not Qualify to gap gauge
Detection Stage Receipt
Problem Severity Function
NG Quantity 9250
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityhead@starprojectsindia.com
Plant Head/CEO Email ID engineering@starprojectsindia.com
MD Email ID ishant@starprojectsindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15000
150000
0
0
0
165000
Check Qty
15000
0
0
0
0
15000
NG Qty
9250
0
0
0
0
9250
 
Scrap 9250
Rework 0
Under Deviation 0
Containment Action
All Material has been hold for 100% Re-Inspection for same with proper identification.
 
3. Process Flow
Process Flow Description
Receipt of Raw Material-Storage of raw material-Melting-PDC-1st Trimming-shot Blasting-1-2nd Trimming-Barreling-Shot Blasting-2-Sound Testing-Stress relieving-Final Inspection & packing-Storage & Dispatch.
 
4. Process Details
Process / Operation Stress Relieving
Outsource No
Machine / Cell Oven-02
Machine / Cell No. No
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodLug Matching SequenceLug Matching Sequence was DisturbX
ManNegligency Done by InspectorSemi-Skilled operator was thereX
ToolReceiving Gauge Wear outBase Size and lug size of slip gauge found at higher point.X
MethodHeating parameter disturbHeating Parameter Observed 261°C against 270±20°CO
MethodReceiving Gauge Validation PlanReceving Gauge Validation Plan was Available but not done ProperlyX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Per Lot
7. Root Cause Analysis (Occurance)
Why 1 Flatness Found NG in core Plate C-101
Why 2 Due to Lug Matching Sequence was Disturb
Why 3 Due to improper material handling during heating
Why 4 Semi-Skilled operator was there
Why 5
Root Cause (Occurance) Due to Lug Matching Sequence was disturbed
 
Root Cause Analysis (Outflow)
Why 1 100% parts was checked by receiving gauge
Why 2 Receiving gauge was not detected the defective parts
Why 3 Due to Base Size and lug size of Receiving gauge found at higher point
Why 4 Receiving Gauge wear out
Why 5
Root Cause (Outflow) Receiving Gauge wear out
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceReceiving gauge validation plan has been updated and adheredAjay Malik10/11/202210/11/2022Completed
OutflowTraining has been provided to Inspectors & OperatorAjay malik09/11/202209/11/2022Completed
OccuranceReceiving Gauge Rectification Has been done..Ajay Malik10/11/202210/11/2022Completed
OccuranceCheck Point added in heating WIAjay Malik10/11/202210/11/2022Completed
OutflowInspectior & Gauger Identification Code has been marked on every BoxesAjay Malik10/11/202210/11/2022Completed
Outflow100% marking Implemented on every lotAjay malik10/11/202210/11/2022Completed
OutflowQuality Alert made and displayed at concerned areaAjay malik09/11/202209/11/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspector & Gauger Identification Code has been marked on every Boxes With 100% Marking on parts
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Per Lot
10. Evidance of Countermeasure
Occurance (Before) Check Point Not added in Heating WI
300_Occurance_Before.pdf
Occurance (After) Check Point added in Heating WI
300_Occurance_After.pdf
Outflow (Before) No Check Point Available for Proper Identification
300_Outflow_Before.pdf
Outflow (After) Inspector & Gauger Identification Code has been marked on every Boxes.
300_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant In All Model of Core Plate
 
12. Document Review
Documents WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission OK