QFR No - 7000884827
Defect Details
NC No. | 7000884827 |
NC Date | 21/12/2022 |
NC Submission Date | |
Part No. | 520CE00502 |
Part Name | CLUTCH SHAFT ASSEMBLY DI ENGINE |
Supplier Name & Code | 200172-AURANGABAD AUTO ENGG PVT LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | M/CING SHIFT.-Key width position shift |
1. Problem Description
Defect Description | Hole Position shift w.r.t key way slot |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 100 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | verma.aaepl@gmail.com |
Plant Head/CEO Email ID | aaepl.pantnagar@sangkaj.com |
MD Email ID | steel@sangkaj.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
280
|
0
|
0
|
0
|
0
|
280
|
Check Qty |
280
|
0
|
0
|
0
|
0
|
280
|
NG Qty |
80
|
0
|
0
|
0
|
0
|
80
|
Scrap | 80 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% WIP rechecked by visual Inspection |
3. Process Flow
Process Flow Description |
---|
Pressing - CNC - Bush pressing - OD grinding - Keyway broaching . |
4. Process Details
Process / Operation | Keyway broaching |
Outsource | No |
Machine / Cell | Broaching Machine |
Machine / Cell No. | Gear Cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Part not located in broaching fixture | Locating pin length short | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Locating hole Dia. 5mm position shift w.r.t. keyway Broaching. |
Why 2 | Keyway Broaching shift during broachng operation. |
Why 3 | Hole not guide in position in pin |
Why 4 | Less Awareness of operator for process |
Why 5 | |
Root Cause (Occurance) | Less Awareness of operator for process. |
Root Cause Analysis (Outflow)
Why 1 | Locating hole Dia. 5mm position shift w.r.t. keyway Broaching. |
Why 2 | Hole w.r.t. Keyway broaching relation gauge done on Sampling basis. |
Why 3 | Hole w.r.t. Keyway broaching relation gauge done on Sampling basis. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Hole w.r.t. Keyway broaching relation gauge done on Sampling basis. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1) Hole guide pin position height incressed from 2mm to 8mm. 2) Concern operator training provided for this defect. | Mr.BAde | 31/12/2022 | 29/12/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1) Hole w.r.t. Keyway broaching relation gauge done on 100%. 2) After Gauge insection 100% visual inspection with identification line marking with marker putted on face. 3)All final inspector training provided for this defect. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Less Awareness of operator for process. 325_Occurance_Before.xlsx |
Occurance (After) |
1) Hole guide pin position height increased from 2mm to 8mm.
2) Concern operator training provided for this defect. 325_Occurance_After.xlsx |
Outflow (Before) |
Hole w.r.t. Keyway broaching relation gauge done on Sampling basis. 325_Outflow_Before.xlsx |
Outflow (After) |
1) Hole w.r.t. Keyway broaching relation gauge done on 100%.
2) After Gauge insection 100% visual inspection with identification line marking with marker putted on face.
3)All final inspector training provided for this defect. 325_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | No |
12. Document Review
Documents | ControlPlan, PokayokeCheckSheet, PFMEA, WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | OK |