QFR No - 7000884827
Defect Details
NC No. 7000884827
NC Date 21/12/2022
NC Submission Date
Part No. 520CE00502
Part Name CLUTCH SHAFT ASSEMBLY DI ENGINE
Supplier Name & Code 200172-AURANGABAD AUTO ENGG PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details M/CING SHIFT.-Key width position shift
 
1. Problem Description
Defect Description Hole Position shift w.r.t key way slot
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 100
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID verma.aaepl@gmail.com
Plant Head/CEO Email ID aaepl.pantnagar@sangkaj.com
MD Email ID steel@sangkaj.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
280
0
0
0
0
280
Check Qty
280
0
0
0
0
280
NG Qty
80
0
0
0
0
80
 
Scrap 80
Rework 0
Under Deviation 0
Containment Action
100% WIP rechecked by visual Inspection
 
3. Process Flow
Process Flow Description
Pressing - CNC - Bush pressing - OD grinding - Keyway broaching .
 
4. Process Details
Process / Operation Keyway broaching
Outsource No
Machine / Cell Broaching Machine
Machine / Cell No. Gear Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolPart not located in broaching fixtureLocating pin length shortO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Locating hole Dia. 5mm position shift w.r.t. keyway Broaching.
Why 2 Keyway Broaching shift during broachng operation.
Why 3 Hole not guide in position in pin
Why 4 Less Awareness of operator for process
Why 5
Root Cause (Occurance) Less Awareness of operator for process.
 
Root Cause Analysis (Outflow)
Why 1 Locating hole Dia. 5mm position shift w.r.t. keyway Broaching.
Why 2 Hole w.r.t. Keyway broaching relation gauge done on Sampling basis.
Why 3 Hole w.r.t. Keyway broaching relation gauge done on Sampling basis.
Why 4
Why 5
Root Cause (Outflow) Hole w.r.t. Keyway broaching relation gauge done on Sampling basis.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1) Hole guide pin position height incressed from 2mm to 8mm. 2) Concern operator training provided for this defect.Mr.BAde31/12/202229/12/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1) Hole w.r.t. Keyway broaching relation gauge done on 100%. 2) After Gauge insection 100% visual inspection with identification line marking with marker putted on face. 3)All final inspector training provided for this defect.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Less Awareness of operator for process.
325_Occurance_Before.xlsx
Occurance (After) 1) Hole guide pin position height increased from 2mm to 8mm. 2) Concern operator training provided for this defect.
325_Occurance_After.xlsx
Outflow (Before) Hole w.r.t. Keyway broaching relation gauge done on Sampling basis.
325_Outflow_Before.xlsx
Outflow (After) 1) Hole w.r.t. Keyway broaching relation gauge done on 100%. 2) After Gauge insection 100% visual inspection with identification line marking with marker putted on face. 3)All final inspector training provided for this defect.
325_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents ControlPlan, PokayokeCheckSheet, PFMEA, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK