QFR No - 7000884966
Defect Details
NC No. 7000884966
NC Date 21/12/2022
NC Submission Date
Part No. 520AE05702
Part Name CORE PLATE - SHINE & UNICORN
Supplier Name & Code 101145-STAR PROJECTS INDIA
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details FLATNESS NOT OK.-Not qualify to gap gaue
 
1. Problem Description
Defect Description Not qualify to gap gauge (Flatness found up to 0.2 mm against 0.1 mm)
Detection Stage Receipt
Problem Severity Function
NG Quantity 1615
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityhead@starprojectsindia.com
Plant Head/CEO Email ID engineering@starprojectsindia.com
MD Email ID ishant@starprojectsindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
8000
23000
46000
0
10000
87000
Check Qty
8000
5000
0
0
4500
17500
NG Qty
1615
211
0
0
8
1834
 
Scrap 1615
Rework 0
Under Deviation 0
Containment Action
All Material has been hold for 100 % Re-inspection with proper identification
 
3. Process Flow
Process Flow Description
Receipt of Raw material+ Storage of raw material+ Hold cum melting +PDC+ First Trimming +Shot Blast+2nd Trimming+ Barreling +Shot blasting+ sound testing+ stress relieving +final inspection & packing +Storage & dispatched
 
4. Process Details
Process / Operation PDC & Final Inspection
Outsource No
Machine / Cell MC-10
Machine / Cell No. MC-10
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNegligency Done by InspectorBaijnath,Rekha,Shyamveer)Training record & Skill amtrix available for same(F13/P&A(OJT),found okO
MachineGap Gauge Wear OutGap Gauge Validation & Verification Plan Available and Adhered (F07/QAD(JFR)O
MethodImproper flatness of stress relieving fixtureFixture validation plan available and adhered(F07A/QAD(JFR)O
MethodTie bar Bolt BalancingTie Baar Bolt Was found Un-BalanceX
MethodImproper Stress relieving ParameterStress relieving Parameter Observed Temp. 261°C against 270±20°C ,Time obsd 30 minutes Against 25±5O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Per Lot
7. Root Cause Analysis (Occurance)
Why 1 Core Plate-C101 Not Qualify to gap gauge
Why 2 One face of the die was found in tapper
Why 3 Tie bar Bolt was found Un-Balance
Why 4 Tie bar Bolt Locking or fix mechanism not available
Why 5 Possibility not considered during define the daily machine check sheet
Root Cause (Occurance) Tie bar Bolt Locking Mechanism Broken
 
Root Cause Analysis (Outflow)
Why 1 Core Plate-C101 Not Qualify to gap gauge
Why 2 100% parts was not passed from gap gauge.
Why 3 Gap gauge set on 2.12 mm but as per existing part calculation should be 2.09 mm
Why 4 Gap gauge size can be change as per part thickness
Why 5 Gap gauge setting frequency not defined
Root Cause (Outflow) Due to Base Size and lug size of Receiving gauge was set at higher Point.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool history to be maintainedAjay Malik26/12/202226/12/2022Completed
Outflow200% inspection started with identification ,Identification also defined for warehouse and star end.Ajay Malik22/12/202222/12/2022Completed
OutflowGap gauge setting & verification started on daily basis as per (15 part avg. thickness +Flatness +Passing allowance 10 microns)Ajay Malik23/12/202223/12/2022Completed
OutflowGap gauge size varification check point added in Pre-Dispatch inspection reportAjay Malik23/12/202223/12/2022Completed
OccuranceDaily Machine check sheet updatedAjay Malik26/12/202226/12/2022Completed
OutflowQuality Alert made and displayed at concerned areaAjay Malik22/12/202222/12/2022Completed
OutflowTraining has been provided to OperatorAjay Malik22/12/202222/12/2022Completed
OccuranceTie Bar Bolt Locking Mechanism to be made and freezedAjay Malik30/12/202230/12/2022Completed
OccuranceTie Bar Bolt Locking Mechanism to be made and freezedAjay Malik22/12/202222/12/2022Completed
Occurance.PDC Tool to be rectified and thickness maintain on 1.95 to 2.00 mm instead of 1.95 ~2.05 mmAjay Malik26/12/202226/12/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Gap gauge setting & verification started on daily basis as per (15 part avg. thickness +Flatness +Passing allowance 10 microns
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Per Lot
10. Evidance of Countermeasure
Occurance (Before) Tie bar Bolt Locking or fix mechanism not available
324_Occurance_Before.pdf
Occurance (After) Tie Bar Bolt Locking Mechanism to be made and freezed
324_Occurance_After.pdf
Outflow (Before) Gap gauge set on 2.12 mm but as per existing part calculation should be 2.09 mm
324_Outflow_Before.pdf
Outflow (After) Gap gauge setting & verification started on daily basis as per (15 part avg. thickness +Flatness + Passing allowance 10 microns)
324_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Models of Core Plate
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission OK