QFR No - 7000890664
Defect Details
NC No. | 7000890664 |
NC Date | 16/01/2023 |
NC Submission Date | |
Part No. | S2BG02502B |
Part Name | BRACKET UN P/C KTEP |
Supplier Name & Code | 100973-TESMO MOTORCAST PRIVATE LIMITE |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | THREADING NOT OK-Threading and Casting Defect |
1. Problem Description
Defect Description | Major & fitment related defects like threading NG, Blow holes, cracks etc. repetitively observed. |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 1100 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | rkhare@tesmomotorcast.com |
Plant Head/CEO Email ID | harish.bala@tesmomotorcast.com |
MD Email ID | svkallani@tesmomotorcast.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1100
|
0
|
0
|
6000
|
13000
|
20100
|
Check Qty |
1100
|
0
|
0
|
6000
|
13000
|
20100
|
NG Qty |
1100
|
0
|
0
|
20
|
0
|
1120
|
Scrap | 20 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Perpendicularity checking gauge made and start hourly checking |
3. Process Flow
Process Flow Description |
---|
PDC - Deburring - Remer - surface treatment - Camper - tapping - Air Cleaning - Packing |
4. Process Details
Process / Operation | PDC |
Outsource | No |
Machine / Cell | 250-2 |
Machine / Cell No. | 2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | core pin hardness not ok | hardness testing report check | O |
Tool | side core not proper open | gauge | O |
Tool | Die Core Side Pin Bend | Perpendicularity gauge | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | Every Hr |
7. Root Cause Analysis (Occurance)
Why 1 | Tap not gone up to required depth |
Why 2 | Tap jam while completing its cycle |
Why 3 | Hole pin perpendicularity not ok |
Why 4 | Die core pin bend |
Why 5 | Pin hardness not as per requirement |
Root Cause (Occurance) | Core pin hardness not freeze. |
Root Cause Analysis (Outflow)
Why 1 | Tap not gone up to required depth |
Why 2 | Tap jam while completing its cycle |
Why 3 | Hole pin perpendicularity not ok |
Why 4 | Die core pin perpendicularity not ok |
Why 5 | Perpendicularity not check |
Root Cause (Outflow) | Core pin Perpendicularity checking frequency not defined. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Hourly pin hole Perpendicularity checking | Rahul | 27/06/2023 | Pending | |
Occurance | Pin hardness freeze | Sachin | 27/06/2023 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Perpendicularity checking started on hourly check on PDC |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 500 |
10. Evidance of Countermeasure
Occurance (Before) |
Threading not OK 331_Occurance_Before.jpeg |
Occurance (After) |
Threading ok 331_Occurance_After.jpeg |
Outflow (Before) |
THREADING NOTOK 331_Outflow_Before.jpeg |
Outflow (After) |
THREADING OK 331_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | kwpk |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | GAUGE CHEKING |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |