QFR No - 7000891491
Defect Details
NC No. 7000891491
NC Date 20/01/2023
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1136-ETL Suspension Sanand
Defect Details MIX UP OTHER MODEL-Mix up Other model
 
1. Problem Description
Defect Description Other model Mixing .
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 250
Is Defect Repeatative? Yes
Defect Sketch / Photo tj5qkjazjfglq5x4xctoxy0m.png
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4000
1250
0
0
0
5250
Check Qty
4000
1250
0
0
0
5250
NG Qty
250
0
0
0
0
250
 
Scrap 250
Rework 0
Under Deviation 0
Containment Action
Segregated all parts at ETL, at Warehouse & at NPC Nabha.
 
3. Process Flow
Process Flow Description
Process Flow Description 1.Raw Material 2.Cutting & Chemfering 3. Multistation Draw 4.Head Formation 5.Rough Grinding 6.Punching 7.CNC Head Turning 8.CNC Boring & Facing 9.Tapping 10. Chemfering 1&2 11.Finish Grinding 12.Final Inspection 13.Cleaning 14.Oiling 15.Packing &Dispatch
 
4. Process Details
Process / Operation Final Inspection
Outsource Yes
Machine / Cell ST-01
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodskipped at final inspectionit was observed that parts skipped during sampling at final inspection.O
Methodwrong part mixed during material handingAfter verification we found material handling properly as per std.O
Machinetempered program run in CnC machineit was observed that no programO
ManPacking person negligence at in packingPacking person was not awareX
ToolTap Wear Outafter verification we found tap was wear outO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Mix up Other model
Why 2 other model box mixed at dispatch station
Why 3 Dispatch helper was not aware
Why 4 different model boxes were placed at same places
Why 5 No identification point was not available for particular model
Root Cause (Occurance) No identification point was not available for particular model
 
Root Cause Analysis (Outflow)
Why 1 Mix up Other model
Why 2 other model box mixed at dispatch station
Why 3 No checkpoint was available after packing
Why 4
Why 5
Root Cause (Outflow) No checkpoint was available after packing
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceGive the awareness training for dispatch departmentMr. Gurpreet singh25/01/202323/01/2023Completed
OutflowNew checkpoint to be added as temporary basis in warehouseMr. Ratness25/01/202324/01/2023Completed
Occuranceidentification point should be available for particular modelMr. Ankush22/01/202321/01/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details new checkpoint add at warehouse
Inspection Method Other
Other Inspection Method visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No identification point was not available for particular model
336_Occurance_Before.jpeg
Occurance (After) Place is define by identification tag for perticular moidel.
336_Occurance_After.png
Outflow (Before) No any check point available after packing.
336_Outflow_Before.png
Outflow (After) New check point establish in warehouse for material check befor dispatch in GIL Sanand Plant.
336_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant K-86 Seat pipe
 
12. Document Review
Documents
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 0
Reason for submission Provide evidence for training record and check point sheet added in warehouse