QFR No - 7000891906
Defect Details
NC No. 7000891906
NC Date 24/01/2023
NC Submission Date
Part No. 520KN00173
Part Name RESERVOIR CAP RAW CASTING
Supplier Name & Code 101032-ASM CASTINGS PRIVATE LIMITED (
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details BLOW HOLES-Blow Hole Damages
 
1. Problem Description
Defect Description BLOW HOLES-Blow Hole Damages
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 8000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@asmcastings.in
Plant Head/CEO Email ID skaul@asmcastings.in
MD Email ID rajiv@asmcastings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
8000
12000
0
8000
2580
30580
Check Qty
8000
12000
0
8000
2580
30580
NG Qty
0
72
0
21
14
107
 
Scrap 107
Rework 0
Under Deviation 0
Containment Action
All Material Re-checked & Dot Marking done on the same for identification.
 
3. Process Flow
Process Flow Description
R.M. Receiving - Die Casting - Fatling - Lancering & Buffing - Drilling -Shot Blasting - Final - Inspection & PDI - Packing -Dispatch.
 
4. Process Details
Process / Operation Die Casting
Outsource No
Machine / Cell Die Casting
Machine / Cell No. PDC-04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine P.M. Not doneP.M. Check Sheet verified & Found OKX
ManNew operatorVerbal Interview taken & Found OKX
ToolDie Life OverDie History Card found OkX
MaterialChemical Composition not okMTC Verified & Found OKX
MethodInspection method not adeqautesingle part inspection not done (4 to 5 parts are kept in hand by inspector & Checked together)O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Blow Holes in Casting
Why 2 Material pouring Method Not ok in PDC Machine
Why 3 Air & Gasses mixed material poured in Production which causes blow holes.
Why 4 Material Pouring Done at the time of Degassing Also
Why 5 Operator not aware about stop production during Degassing. (No Training /Q-Alert Available for the Same)
Root Cause (Occurance) Training not provided to operator for Stopping production during degassing process.
 
Root Cause Analysis (Outflow)
Why 1 Inspection Method not adequate
Why 2 Single part Inspection not done by Inspector (4 to 5 Part checked at once which causes flow of NG Parts)
Why 3 Inspector Not aware about singe part inspection
Why 4 Check Point not added in Work Instruction for single Part Inspection
Why 5
Root Cause (Outflow) Check Point not added in Work Instruction for single Part Inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTraining Provided to Operators for Stopping production during degassingLalit Sahrma01/02/202301/02/2023Completed
OutflowCheck point added in Work Instruction for Single Part Inspection .Ateev Sharma01/02/202301/02/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Single Part Inspection started in-place of 4 to 05 parts in final inspection.
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Operator was not aware about Stopping Production during Degassing.
350_Occurance_Before.pdf
Occurance (After) Training Provided to Operators for Stopping production during Degassing.
350_Occurance_After.pdf
Outflow (Before) check point was not available in W.I. for Single part Inspection
350_Outflow_Before.pdf
Outflow (After) Check Point added in W.I. for Single Part Inspection.
350_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant PDC
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document Training Record
 
13. Effectiveness Of Action
Reviewed Quantity 24000
Reason for submission No defect found in 3 lot