QFR No - 7000903135
Defect Details
NC No. 7000903135
NC Date 17/03/2023
NC Submission Date
Part No. S2MX00112B
Part Name STEEL BUSH
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details LENGTH UNDERSIZE-Length Undersize up to 0.5mm
 
1. Problem Description
Defect Description Length observed up to 23.30mm against 24-0.20mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 10000
Is Defect Repeatative? Yes
Defect Sketch / Photo vhasrjzr11exfzffeuow2hrz.jpg
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
0
3000
2000
15000
Check Qty
10000
0
0
3000
2000
15000
NG Qty
40
0
0
0
0
40
 
Scrap 30
Rework 10
Under Deviation 0
Containment Action
All Finish Good Customer End and Godown Material Return call
 
3. Process Flow
Process Flow Description
1)RM Inward-2)store- 3)Parting-4)2nd side ID Chamfer-5) Plating -6) Final Inspection -7) Dispatch .
 
4. Process Details
Process / Operation Parting
Outsource Yes
Machine / Cell Traub /Traub Cell
Machine / Cell No. Traub No.2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRandomly Bend Pipe Mix with OK RM2 pipe found Bend Out of 60 PipesX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 no.s/hr
7. Root Cause Analysis (Occurance)
Why 1 Length Under Size
Why 2 During Traub parting process RM pipe was not Move
Why 3 Finger ok But Not Open on Time After part cutting
Why 4 RM Pipe Bend
Why 5
Root Cause (Occurance) RM PIPE BEND
 
Root Cause Analysis (Outflow)
Why 1 Length Under Size
Why 2 Defected piece mix with ok material During final inspection
Why 3 Inspector mistake
Why 4 During final inspection Defected part bag and ok FG bag kept one Location
Why 5
Root Cause (Outflow) Defected piece mix with ok material During final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOCCURANCE- All Bend Pipe Segregation Before machining, OUTFLOWS- Separate area Decide on Final Inspection Table.Dispatch Engineer31/03/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection Table modification for NG Parts Red Box Provide and finish Good Regular Polybag
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) RM Pipe Bend
389_Occurance_Before.jpeg
Occurance (After) All Suspected bend RM Pipe Material Segregation /
389_Occurance_After.jpeg
Outflow (Before) During final inspection Defected part bag and ok FG bag kept one Location
389_Outflow_Before.jpeg
Outflow (After) Inspection Table modification for NG Parts Red Box Provide and finish Good Regular Polybag
389_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Steel Bush
 
12. Document Review
Documents PMCheckSheet, PFMEA, WISOP
Specify Other Document Final Inspection QP
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission OK