QFR No - 7000903135
Defect Details
NC No. | 7000903135 |
NC Date | 17/03/2023 |
NC Submission Date | |
Part No. | S2MX00112B |
Part Name | STEEL BUSH |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1143-ETL Suspension Halol, Vadodara |
Defect Details | LENGTH UNDERSIZE-Length Undersize up to 0.5mm |
1. Problem Description
Defect Description | Length observed up to 23.30mm against 24-0.20mm |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 10000 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | vhasrjzr11exfzffeuow2hrz.jpg |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | production@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
0
|
0
|
3000
|
2000
|
15000
|
Check Qty |
10000
|
0
|
0
|
3000
|
2000
|
15000
|
NG Qty |
40
|
0
|
0
|
0
|
0
|
40
|
Scrap | 30 |
Rework | 10 |
Under Deviation | 0 |
Containment Action |
---|
All Finish Good Customer End and Godown Material Return call |
3. Process Flow
Process Flow Description |
---|
1)RM Inward-2)store- 3)Parting-4)2nd side ID Chamfer-5) Plating -6) Final Inspection -7) Dispatch . |
4. Process Details
Process / Operation | Parting |
Outsource | Yes |
Machine / Cell | Traub /Traub Cell |
Machine / Cell No. | Traub No.2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Randomly Bend Pipe Mix with OK RM | 2 pipe found Bend Out of 60 Pipes | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 no.s/hr |
7. Root Cause Analysis (Occurance)
Why 1 | Length Under Size |
Why 2 | During Traub parting process RM pipe was not Move |
Why 3 | Finger ok But Not Open on Time After part cutting |
Why 4 | RM Pipe Bend |
Why 5 | |
Root Cause (Occurance) | RM PIPE BEND |
Root Cause Analysis (Outflow)
Why 1 | Length Under Size |
Why 2 | Defected piece mix with ok material During final inspection |
Why 3 | Inspector mistake |
Why 4 | During final inspection Defected part bag and ok FG bag kept one Location |
Why 5 | |
Root Cause (Outflow) | Defected piece mix with ok material During final inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | OCCURANCE- All Bend Pipe Segregation Before machining, OUTFLOWS- Separate area Decide on Final Inspection Table. | Dispatch Engineer | 31/03/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection Table modification for NG Parts Red Box Provide and finish Good Regular Polybag |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
RM Pipe Bend 389_Occurance_Before.jpeg |
Occurance (After) |
All Suspected bend RM Pipe Material Segregation / 389_Occurance_After.jpeg |
Outflow (Before) |
During final inspection Defected part bag and ok FG bag kept one Location 389_Outflow_Before.jpeg |
Outflow (After) |
Inspection Table modification for NG Parts Red Box Provide and finish Good Regular Polybag 389_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Steel Bush |
12. Document Review
Documents | PMCheckSheet, PFMEA, WISOP |
Specify Other Document | Final Inspection QP |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | OK |