QFR No - 7000911552
Defect Details
NC No. | 7000911552 |
NC Date | 26/04/2023 |
NC Submission Date | |
Part No. | S2AB01907B |
Part Name | ADJUSTER POWDER COATED |
Supplier Name & Code | 100973-TESMO MOTORCAST PRIVATE LIMITE |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | EXCESS MATERIAL-excess material at spring resting face |
1. Problem Description
Defect Description | Major power coating defects observed with casting concern also. |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1200 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | rkhare@tesmomotorcast.com |
Plant Head/CEO Email ID | harish.bala@tesmomotorcast.com |
MD Email ID | svkallani@tesmomotorcast.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3200
|
0
|
4200
|
3000
|
6000
|
16400
|
Check Qty |
3200
|
0
|
0
|
3000
|
6000
|
12200
|
NG Qty |
1200
|
0
|
0
|
0
|
0
|
1200
|
Scrap | 1200 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Check point added in final stage. |
3. Process Flow
Process Flow Description |
---|
PDC-REAMER-GRINDING-SURFACE TREATMENT-INSPECTION-POWDER COATING-SAMPLE INSPECTION-PACKING DESPATCH |
4. Process Details
Process / Operation | PDC |
Outsource | No |
Machine / Cell | PDC-350 Ton |
Machine / Cell No. | PDC-5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Ejector Pin dia oversize | pin bend dia oversize & excess Flash generated | O |
Tool | pin jam in die | pin dia oversize due to heat generation | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual checking |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1 |
7. Root Cause Analysis (Occurance)
Why 1 | PIN FLASH ON SPRING RESTING FACE |
Why 2 | EJECTOR PIN DIE INCREASE ON INSERT |
Why 3 | DIE RUNNING WITH UNBALANCE EJECTION |
Why 4 | SETTING NOT DONE CORRECTLY |
Why 5 | POOR SKILL LEVEL |
Root Cause (Occurance) | EJECTOR SETTING SKILL LEVEL NOT GOOD |
Root Cause Analysis (Outflow)
Why 1 | PIN FLASH ON SPRING RESTING FACE |
Why 2 | PIN FLASH CHECKING MISSED BY INSPECTOR |
Why 3 | IMPROPER TRAINING TO INSPECTOR |
Why 4 | VISUAL DISPLAY NOT AVAILABLE |
Why 5 | |
Root Cause (Outflow) | VISUAL DISPLAY OF PIN FLASH NOT AVAILABLE |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | VISUAL DISPLAY AT INSPECTION WITH PROPER TRAINING | ANKUSH | 30/06/2023 | 30/06/2023 | Completed |
Occurance | PIN AND INSERT DIAMETER CHECKING | SACHIN | 01/07/2023 | 01/07/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | VISUAL DISPLAY IN INSPECTION TABLE WITH SAMPLES |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1 |
10. Evidance of Countermeasure
Occurance (Before) |
PART WITH PIN FLASH 442_Occurance_Before.jpeg |
Occurance (After) |
EJECTOR PIN DIA INCREASE 442_Occurance_After.jpeg |
Outflow (Before) |
PART WITH PIN FLASH 442_Outflow_Before.jpeg |
Outflow (After) |
SAMPLE PLACED ON FINAL STAGE 442_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | PART DISPLAY |
13. Effectiveness Of Action
Reviewed Quantity | 10 |
Reason for submission | Corrective action parts submission. |