QFR No - 7000920866
Defect Details
NC No. 7000920866
NC Date 09/06/2023
NC Submission Date
Part No. 538FL00102
Part Name PISTON NUT - WP
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details EXCESS MATERIAL-DO BURR
 
1. Problem Description
Defect Description Burr found on hex
Detection Stage Receipt
Problem Severity Function
NG Quantity 1889
Is Defect Repeatative? No
Defect Sketch / Photo 2qwja5mj5mgg3izzjrxtdfil.jpg
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2400
0
0
600
0
3000
Check Qty
2400
0
0
600
0
3000
NG Qty
1889
0
0
0
0
1889
 
Scrap 0
Rework 1889
Under Deviation 0
Containment Action
All Suspected Material Segregation at Customer End
 
3. Process Flow
Process Flow Description
Forging Finish Inward -Raw Material Store- CNC-1- CNC-2- Plating- Final Inspection - Packing - Dispatch -
 
4. Process Details
Process / Operation CNC-1&2
Outsource No
Machine / Cell CNC-13
Machine / Cell No. CNC section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolInsert Corner WearInsert Run Than decide tool lifeO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1005
7. Root Cause Analysis (Occurance)
Why 1 Burr found on hex
Why 2 Excess Burr Sticking at Across Corner Area
Why 3 During CNC process Across Corner Area Excess Material Not removed.
Why 4
Why 5
Root Cause (Occurance) During CNC process Across Corner Area Excess Material Not removed.
 
Root Cause Analysis (Outflow)
Why 1 Burr found on hex
Why 2 During Sampling Burr effected Material Not Detected
Why 3
Why 4
Why 5
Root Cause (Outflow) During Sampling Burr effected Material Not Detected
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDeburring Process Add After Both CNC OperationPlant Head01/07/202303/07/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Visual Inspection Instead Of Sampling inspection.
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Before - After CNC Process Deburring not Done to Every Part Only Heavy excess Burr Part Deburring.
470_Occurance_Before.docx
Occurance (After) 100% Deburring Process Start Each Part after CNC Process
470_Occurance_After.docx
Outflow (Before) Sampling Visual Inspection
470_Outflow_Before.docx
Outflow (After) 100% Visual Inspection Start Before Dispatch .
470_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Spacer Tubes
 
12. Document Review
Documents ControlPlan, PFMEA, ProcessFlowChart
Specify Other Document Nil
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission no any issue observed after action submitted.