QFR No - 7000920866
Defect Details
NC No. | 7000920866 |
NC Date | 09/06/2023 |
NC Submission Date | |
Part No. | 538FL00102 |
Part Name | PISTON NUT - WP |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | EXCESS MATERIAL-DO BURR |
1. Problem Description
Defect Description | Burr found on hex |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 1889 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | 2qwja5mj5mgg3izzjrxtdfil.jpg |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2400
|
0
|
0
|
600
|
0
|
3000
|
Check Qty |
2400
|
0
|
0
|
600
|
0
|
3000
|
NG Qty |
1889
|
0
|
0
|
0
|
0
|
1889
|
Scrap | 0 |
Rework | 1889 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected Material Segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
Forging Finish Inward -Raw Material Store- CNC-1- CNC-2- Plating- Final Inspection - Packing - Dispatch - |
4. Process Details
Process / Operation | CNC-1&2 |
Outsource | No |
Machine / Cell | CNC-13 |
Machine / Cell No. | CNC section |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Insert Corner Wear | Insert Run Than decide tool life | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1005 |
7. Root Cause Analysis (Occurance)
Why 1 | Burr found on hex |
Why 2 | Excess Burr Sticking at Across Corner Area |
Why 3 | During CNC process Across Corner Area Excess Material Not removed. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | During CNC process Across Corner Area Excess Material Not removed. |
Root Cause Analysis (Outflow)
Why 1 | Burr found on hex |
Why 2 | During Sampling Burr effected Material Not Detected |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | During Sampling Burr effected Material Not Detected |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Deburring Process Add After Both CNC Operation | Plant Head | 01/07/2023 | 03/07/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Visual Inspection Instead Of Sampling inspection. |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Before - After CNC Process Deburring not Done to Every Part Only Heavy excess Burr Part Deburring. 470_Occurance_Before.docx |
Occurance (After) |
100% Deburring Process Start Each Part after CNC Process 470_Occurance_After.docx |
Outflow (Before) |
Sampling Visual Inspection 470_Outflow_Before.docx |
Outflow (After) |
100% Visual Inspection Start Before Dispatch . 470_Outflow_After.docx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Spacer Tubes |
12. Document Review
Documents | ControlPlan, PFMEA, ProcessFlowChart |
Specify Other Document | Nil |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | no any issue observed after action submitted. |