QFR No - 7000933342
Defect Details
NC No. 7000933342
NC Date 28/07/2023
NC Submission Date
Part No. F2DZ08810B
Part Name K0PG FORK BOLT
Supplier Name & Code 101037-SHREE PATEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details RUSTY-White rust
 
1. Problem Description
Defect Description Rust
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 450
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality_spi@rediffmail.com
Plant Head/CEO Email ID planthead_spi@rediffmail.com
MD Email ID rspatel_spi@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4480
0
0
0
0
4480
Check Qty
4480
0
0
0
0
4480
NG Qty
450
0
0
0
0
450
 
Scrap 450
Rework 0
Under Deviation 0
Containment Action
All suspected part checked and rejected part scraped.
 
3. Process Flow
Process Flow Description
10. Incoming RM 20. Traub Turning 30. CNC 1st set up 40. CNC 2nd set up 50. Plating 60. Inspection 70. Packing & Dispatch
 
4. Process Details
Process / Operation Plating
Outsource No
Machine / Cell Plating Tank
Machine / Cell No. Tank No.1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachinePassivation bath tankDuring process verification passivation bath tank capacity found ok .O
ManUnskilled HelperSkill matrix verified and all the operators and helper found on required level 2 and level 3.O
MachineCurrent fluctuations of rectifierNo any current flucations during the process visit and last month recorded data verified for currenO
MachineWorking on low temperatureTemperature monitoring data verified and found okO
MaterialPlating PassivationDuring process verification plating passivation pH found okO
MethodMaterial HandlingDuring process verification, input and output of parts storage is proper and handle done as per defO
MethodImproper method of drying after platingManual drying procedure not properly maintain by the operator as per given WI of drying.X
ManAwareness of operatorOperator was aware with the defects which can be generate due to improper cleaning .O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
7. Root Cause Analysis (Occurance)
Why 1 White rust/spot part reached at customer end.
Why 2 White rust generated at plating
Why 3 Plating part drying method improper.
Why 4 Plating part hanging with jig and dry with Manual dryer
Why 5
Root Cause (Occurance) While drying the part, the moisture and particle applied on the part catches white rust
 
Root Cause Analysis (Outflow)
Why 1 Heavy rust observed customer end.
Why 2 Inspector not detected dull plated part during final inspection .
Why 3 Inspector was not aware about the defect.
Why 4 No inspection std available at final inspection station.
Why 5
Root Cause (Outflow) No inspection std available at final inspection station.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWe will improve the drying process by introduce industrial drying oven to remove all the moisture from the part.SPI18/11/202304/08/2023Completed
Outflow1)Training provided to the final inspector about the problem and inspection std. 2)The visual inspection frequency increase till installation. 3)New fire wall station will be introduce at final inspection for this kind of defect.SPI04/08/202304/08/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No
Inspection Method Other
Other Inspection Method No
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) Hanger Photo
512_Occurance_Before.pdf
Occurance (After) Industrial drying oven will be introduce after plating for drying.
512_Occurance_After.pdf
Outflow (Before) No inspection std available at final inspection station
512_Outflow_Before.pdf
Outflow (After) 1)Training provided to the final inspector about the problem and inspection std. 2)The visual inspection frequency increase till installation. 3)New fire wall station will be introduce at final inspection for this kind of defect.
512_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Fork Bolt K86A
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document Yes
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission