QFR No - 7000933352
Defect Details
NC No. | 7000933352 |
NC Date | 28/07/2023 |
NC Submission Date | |
Part No. | S1AB00612B |
Part Name | ADJUSTER PLATED |
Supplier Name & Code | 100782-NICE STEEL INDUSTRIES |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | DIAMETER OVER SIZE-ID Oversize |
1. Problem Description
Defect Description | ID oversize found 31.50 mm against specification (30.50~30.70) |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 1601 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | ppc.nice@batragroup.biz |
Plant Head/CEO Email ID | ho.nice@batragroup.biz |
MD Email ID | hitesh@batragroup.biz |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
4000
|
0
|
2000
|
2000
|
11000
|
Check Qty |
3000
|
4000
|
0
|
2000
|
2000
|
11000
|
NG Qty |
45
|
10
|
0
|
0
|
0
|
55
|
Scrap | 55 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material segregated and rejection part scarped |
3. Process Flow
Process Flow Description |
---|
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 BROACHING 120 HEAD GRINDING 130 OUTSIDE MOVEMENT FOR PLATING 140 STORAGE & RQC INSP. OF PLATED MATERIAL 150 FINAL INSPECTION 160 PACKING & DISPATCH |
4. Process Details
Process / Operation | ID sizing |
Outsource | No |
Machine / Cell | Press machine |
Machine / Cell No. | Press machine |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Wrong material used | MTC verified and found ok | O |
Tool | ID sizing punch | ID sizing punched checked and found NG | X |
Method | SOP not followed | SOP available and followed | O |
Man | Unskilled operator | Skill matrix available | O |
Machine | Machine capacity was not ok | Machine capacity is ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | visual |
7. Root Cause Analysis (Occurance)
Why 1 | ID oversize observed |
Why 2 | id not maintained in part at upper size |
Why 3 | leg was open during id sizing |
Why 4 | Extra force on part by ID sizing punch |
Why 5 | Minor welding bead stuck in part - |
Root Cause (Occurance) | leg was open during id sizing |
Root Cause Analysis (Outflow)
Why 1 | Defective part passed to customer |
Why 2 | Could not detect during inspection |
Why 3 | Only go side inspection done by gauge |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Only go side inspection done by gauge |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Re Round process added to close the open legs | Subodh Upadhyay | 20/08/2023 | 20/08/2023 | Completed |
Outflow | Go and No Go gauge to be made | Nimit | 20/08/2023 | 20/08/2023 | Completed |
Outflow | OPL dispalyed | Prahlad | 20/08/2023 | 20/08/2023 | Completed |
Outflow | Training provided to all concern person | Nimit Prakash | 20/08/2023 | 20/08/2023 | Completed |
Occurance | ID punch size decreased | Nimit Prakash | 20/08/2023 | 20/08/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | GO and No go gauge implemented |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
PFD DOCUEMNT 513_Occurance_Before.xlsx |
Occurance (After) |
PFD DOCUEMNT REVISED 513_Occurance_After.jpeg |
Outflow (Before) |
GAUGE 513_Outflow_Before.jpeg |
Outflow (After) |
GAUGE REVISED 513_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | POWER PRESS |
12. Document Review
Documents | ControlPlan, ProcessFlowChart |
Specify Other Document | PFD AND CP UPDATED |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |