QFR No - 7000933352
Defect Details
NC No. 7000933352
NC Date 28/07/2023
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIAMETER OVER SIZE-ID Oversize
 
1. Problem Description
Defect Description ID oversize found 31.50 mm against specification (30.50~30.70)
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1601
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
4000
0
2000
2000
11000
Check Qty
3000
4000
0
2000
2000
11000
NG Qty
45
10
0
0
0
55
 
Scrap 55
Rework 0
Under Deviation 0
Containment Action
All material segregated and rejection part scarped
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 BROACHING 120 HEAD GRINDING 130 OUTSIDE MOVEMENT FOR PLATING 140 STORAGE & RQC INSP. OF PLATED MATERIAL 150 FINAL INSPECTION 160 PACKING & DISPATCH
 
4. Process Details
Process / Operation ID sizing
Outsource No
Machine / Cell Press machine
Machine / Cell No. Press machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWrong material usedMTC verified and found okO
ToolID sizing punchID sizing punched checked and found NGX
MethodSOP not followedSOP available and followedO
ManUnskilled operatorSkill matrix availableO
MachineMachine capacity was not okMachine capacity is okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size visual
7. Root Cause Analysis (Occurance)
Why 1 ID oversize observed
Why 2 id not maintained in part at upper size
Why 3 leg was open during id sizing
Why 4 Extra force on part by ID sizing punch
Why 5 Minor welding bead stuck in part -
Root Cause (Occurance) leg was open during id sizing
 
Root Cause Analysis (Outflow)
Why 1 Defective part passed to customer
Why 2 Could not detect during inspection
Why 3 Only go side inspection done by gauge
Why 4
Why 5
Root Cause (Outflow) Only go side inspection done by gauge
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceRe Round process added to close the open legsSubodh Upadhyay20/08/202320/08/2023Completed
OutflowGo and No Go gauge to be madeNimit20/08/202320/08/2023Completed
OutflowOPL dispalyedPrahlad20/08/202320/08/2023Completed
OutflowTraining provided to all concern personNimit Prakash20/08/202320/08/2023Completed
OccuranceID punch size decreasedNimit Prakash20/08/202320/08/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details GO and No go gauge implemented
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) PFD DOCUEMNT
513_Occurance_Before.xlsx
Occurance (After) PFD DOCUEMNT REVISED
513_Occurance_After.jpeg
Outflow (Before) GAUGE
513_Outflow_Before.jpeg
Outflow (After) GAUGE REVISED
513_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant POWER PRESS
 
12. Document Review
Documents ControlPlan, ProcessFlowChart
Specify Other Document PFD AND CP UPDATED
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission