QFR No - 7000936274
Defect Details
NC No. 7000936274
NC Date 10/08/2023
NC Submission Date
Part No. 520AE00300
Part Name CORE PLATE 3W 4S
Supplier Name & Code 100959-AAR CEE ENGINEERING WORKS UNIT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details FLATNESS NOT OK.-flatness obs 0.30 against 0.10 mm
 
1. Problem Description
Defect Description 3W4S Core Plate Not qualify to gap gauge (Flatness found oversize up to 0.3 mm against 0.1 mm)
Detection Stage Receipt
Problem Severity Function
NG Quantity 10000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc@aarceeengg.com
Plant Head/CEO Email ID planthead.diecasting@aarceeengg.com
MD Email ID vaibhav.arora@aarceeengg.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
16000
0
0
7000
0
23000
Check Qty
16000
0
0
7000
0
23000
NG Qty
1200
0
0
55
0
1255
 
Scrap 0
Rework 1255
Under Deviation 0
Containment Action
Material segregated at the customer end(ETL end) & our end (AAR CEE end)NG parts to be re-shot Blasting
 
3. Process Flow
Process Flow Description
10.Receipt of raw material 20.Storage of raw material 30.Holding cum melting 40. PDC stage 50.Trimming process 60.Shot Blasting 70. Barrelling process 80.Sound Testing 90.stress reliving 100.Final inspection 110.Storage & Dispatch
 
4. Process Details
Process / Operation 60.Shot blasting & 100. Final inspection
Outsource No
Machine / Cell Shot blasting machine
Machine / Cell No. SBM-02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper shot size used at shot blastingObsed SS 0.30 mm shotO
Manskipped at final inspectionok limit sample not displayed at final inspection tableX
MethodImproper stress reliving processChecked and found fixture flatness found up to 0.35 mmX
MethodImproper cycle time at shot blastingFound ok ,6 minutes against 5~7 minutesO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 pcs/lot
7. Root Cause Analysis (Occurance)
Why 1 FLATNESS NOT OK.-flatness obs 0.30 against 0.10
Why 2 shot blasting is not done as per defined frequency.
Why 3 process parameter monitoring not done.
Why 4 lack of awareness of operator
Why 5
Root Cause (Occurance) process parameter monitoring not done.
 
Root Cause Analysis (Outflow)
Why 1 FLATNESS NOT OK.-flatness obs 0.30 against 0.10
Why 2 NG pieces were skipped by final inspection.
Why 3 limit sample not displayed in final inspection area.
Why 4
Why 5
Root Cause (Outflow) limit sample not displayed in final inspection area.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceQC inspection given to the tanningMukesh01/09/202301/09/2023Completed
OutflowOK LIMIT SAMPLE DISPLAY AT FINAL INSPECTION AREAMUKESH03/09/202301/09/2023Completed
OccuranceFixture correctedAjay Malik20/10/202320/10/2023Completed
OccuranceHeating Fixture validation plan made and adhere forAjay Malik23/10/202323/10/2023Completed
OutflowStandard operating procedure made and adhere for gap gauge verification & handlingAjay Malik23/10/202323/10/2023Completed
OutflowStandard operating procedure made and adhere for gap gauge verification & handlingAjay Malik23/10/202323/10/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no change
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10 pcs 1 h
10. Evidance of Countermeasure
Occurance (Before) FORMAT AVAILABLE BUT NOT UPDATED
524_Occurance_Before.pdf
Occurance (After) GIVEN TANNING AND RECORDED STARTED
524_Occurance_After.pdf
Outflow (Before) LIMIT SAMPLE NOT DISPLAYED
524_Outflow_Before.jpg
Outflow (After) LIMIT SAMPLE DISPLAY
524_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission Repeated Occurrence at ETL end -Gap Inspection activity need to strengthen