QFR No - 7000936274
Defect Details
NC No. | 7000936274 |
NC Date | 10/08/2023 |
NC Submission Date | |
Part No. | 520AE00300 |
Part Name | CORE PLATE 3W 4S |
Supplier Name & Code | 100959-AAR CEE ENGINEERING WORKS UNIT |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | FLATNESS NOT OK.-flatness obs 0.30 against 0.10 mm |
1. Problem Description
Defect Description | 3W4S Core Plate Not qualify to gap gauge (Flatness found oversize up to 0.3 mm against 0.1 mm) |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 10000 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qc@aarceeengg.com |
Plant Head/CEO Email ID | planthead.diecasting@aarceeengg.com |
MD Email ID | vaibhav.arora@aarceeengg.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
16000
|
0
|
0
|
7000
|
0
|
23000
|
Check Qty |
16000
|
0
|
0
|
7000
|
0
|
23000
|
NG Qty |
1200
|
0
|
0
|
55
|
0
|
1255
|
Scrap | 0 |
Rework | 1255 |
Under Deviation | 0 |
Containment Action |
---|
Material segregated at the customer end(ETL end) & our end (AAR CEE end)NG parts to be re-shot Blasting |
3. Process Flow
Process Flow Description |
---|
10.Receipt of raw material 20.Storage of raw material 30.Holding cum melting 40. PDC stage 50.Trimming process 60.Shot Blasting 70. Barrelling process 80.Sound Testing 90.stress reliving 100.Final inspection 110.Storage & Dispatch |
4. Process Details
Process / Operation | 60.Shot blasting & 100. Final inspection |
Outsource | No |
Machine / Cell | Shot blasting machine |
Machine / Cell No. | SBM-02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Improper shot size used at shot blasting | Obsed SS 0.30 mm shot | O |
Man | skipped at final inspection | ok limit sample not displayed at final inspection table | X |
Method | Improper stress reliving process | Checked and found fixture flatness found up to 0.35 mm | X |
Method | Improper cycle time at shot blasting | Found ok ,6 minutes against 5~7 minutes | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 pcs/lot |
7. Root Cause Analysis (Occurance)
Why 1 | FLATNESS NOT OK.-flatness obs 0.30 against 0.10 |
Why 2 | shot blasting is not done as per defined frequency. |
Why 3 | process parameter monitoring not done. |
Why 4 | lack of awareness of operator |
Why 5 | |
Root Cause (Occurance) | process parameter monitoring not done. |
Root Cause Analysis (Outflow)
Why 1 | FLATNESS NOT OK.-flatness obs 0.30 against 0.10 |
Why 2 | NG pieces were skipped by final inspection. |
Why 3 | limit sample not displayed in final inspection area. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | limit sample not displayed in final inspection area. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | QC inspection given to the tanning | Mukesh | 01/09/2023 | 01/09/2023 | Completed |
Outflow | OK LIMIT SAMPLE DISPLAY AT FINAL INSPECTION AREA | MUKESH | 03/09/2023 | 01/09/2023 | Completed |
Occurance | Fixture corrected | Ajay Malik | 20/10/2023 | 20/10/2023 | Completed |
Occurance | Heating Fixture validation plan made and adhere for | Ajay Malik | 23/10/2023 | 23/10/2023 | Completed |
Outflow | Standard operating procedure made and adhere for gap gauge verification & handling | Ajay Malik | 23/10/2023 | 23/10/2023 | Completed |
Outflow | Standard operating procedure made and adhere for gap gauge verification & handling | Ajay Malik | 23/10/2023 | 23/10/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | no change |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 10 pcs 1 h |
10. Evidance of Countermeasure
Occurance (Before) |
FORMAT AVAILABLE BUT NOT UPDATED 524_Occurance_Before.pdf |
Occurance (After) |
GIVEN TANNING AND RECORDED STARTED 524_Occurance_After.pdf |
Outflow (Before) |
LIMIT SAMPLE NOT DISPLAYED 524_Outflow_Before.jpg |
Outflow (After) |
LIMIT SAMPLE DISPLAY 524_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 10000 |
Reason for submission | Repeated Occurrence at ETL end -Gap Inspection activity need to strengthen |