QFR No - 7000940002
Defect Details
NC No. | 7000940002 |
NC Date | 25/08/2023 |
NC Submission Date | |
Part No. | S2BG04102B |
Part Name | BRACKET UNCOATED |
Supplier Name & Code | 100959-AAR CEE ENGINEERING WORKS UNIT |
ETL Plant | 1126-ETL Pantnagar |
Defect Details | POROSITY-Failed in Load Testing |
1. Problem Description
Defect Description | Bracket Failed in Breaking Load Test |
Detection Stage | Receipt |
Problem Severity | Safety |
NG Quantity | 1200 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qc@aarceeengg.com |
Plant Head/CEO Email ID | planthead.diecasting@aarceeengg.com |
MD Email ID | vaibhav.arora@aarceeengg.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2800
|
19000
|
0
|
0
|
0
|
21800
|
Check Qty |
2800
|
10000
|
0
|
0
|
0
|
12800
|
NG Qty |
2
|
0
|
0
|
0
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material send back to Aar cee for 100 % inspection with identification |
3. Process Flow
Process Flow Description |
---|
RM Store + Melting cum holding+ HPDC+ Fettling + Reaming + Drilling + Tapping + Final Inspection+ Packing & Dispatch |
4. Process Details
Process / Operation | HPDC & Final Inspection |
Outsource | No |
Machine / Cell | Mc -07 |
Machine / Cell No. | mc-07 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | improper check load | checked and found pin using of 21 mm in the 22 inner dia during load testing in BKT 4102 | X |
Material | Improper material used | Material found ok | O |
Man | unskilled inspector deputed at final inspection | Found ok ,Kaushal inspector was aware about all defects | O |
Method | Improper degassing | manual degassing done ,but not enough chance of porosity in bracket | X |
Method | Error in UTM | Found ok ,calibration done on 1.6.23 and due on 1.6.24 | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Load testing on UTM |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 nos /lot |
7. Root Cause Analysis (Occurance)
Why 1 | 4102 Bracket failed in load testing |
Why 2 | 20 mm pin used in the 22 inner dia of 4102 bracket during load testing |
Why 3 | model wise Pin not defined for load testing in bracket |
Why 4 | Possibility Pin dim. of UTM fixture not considered during development |
Why 5 | |
Root Cause (Occurance) | Possibility Pin dim. of UTM fixture not considered during development |
Root Cause Analysis (Outflow)
Why 1 | 4102 Bracket failed in load testing |
Why 2 | Single pin used for load testing in bracket |
Why 3 | Pin not defined for model wise (Inner dia) |
Why 4 | Check point not covered in work instruction of UTM |
Why 5 | |
Root Cause (Outflow) | Check Point not covered in work instruction of UTM |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Density index ,vaccumization unit & auto plunger lubrication machines introduced | Bhim Singh | 03/09/2023 | 03/09/2023 | Completed |
Occurance | Fixture pin to be made model wise for bracket load testing | Bhim Singh | 04/09/2023 | 04/09/2023 | Completed |
Occurance | N2 degasser introduced and adhered to avoid porosity issue | Bhim Singh | 03/09/2023 | 03/09/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Pin changed and check point added in load testing work instruction Inspection started with identification |
Inspection Method | Other |
Other Inspection Method | UTM + Fixture |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 05 nos/lot |
10. Evidance of Countermeasure
Occurance (Before) |
N/A 534_Occurance_Before.png |
Occurance (After) |
N2 degasser, density index ,vacumization unit and auto plunger lubrication added and started 534_Occurance_After.png |
Outflow (Before) |
N/A 534_Outflow_Before.png |
Outflow (After) |
OPL made and adhered for load testing
Pin made and adhered for model wise bracket for load testing 534_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All bracket model |
12. Document Review
Documents | WISOP |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 0 |
Reason for submission | Please review the possible causes and provided proper action with actual quantity |