QFR No - 7000943533
Defect Details
NC No. | 7000943533 |
NC Date | 11/09/2023 |
NC Submission Date | |
Part No. | 520FG13402 |
Part Name | PRIMARY GEAR ASSEMBLY_ATUL AUTO |
Supplier Name & Code | 100985-IGL INDUSTRIES LIMITED |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | DIMETER UNDERSIZE-rusty issue & boss hight obs 24.03 mm |
1. Problem Description
Defect Description | OPD found undersize up to 124.36~124.51 mm against 124.6±0.035 mm |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 136 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qa@indsur.in |
Plant Head/CEO Email ID | pcwadile@indsur.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
90
|
0
|
0
|
57
|
0
|
147
|
Check Qty |
87
|
0
|
0
|
56
|
0
|
143
|
NG Qty |
3
|
0
|
0
|
1
|
0
|
4
|
Scrap | 4 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Parts segregated at ET and IGL. |
3. Process Flow
Process Flow Description |
---|
Blanks receipt - Hobbing - Shaving - Heat treatment - ID grinding - bush fitting - 0D & ID grinding - Teeth chamfering - Washing - Final inspection - oiling and packing - Dispatch |
4. Process Details
Process / Operation | Grainding |
Outsource | No |
Machine / Cell | Granding Cell |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | excess offset given by operator during correction | excess Offset given by operator during correction | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Height & Dia Under size |
Why 2 | Off-set not provided properly |
Why 3 | More offset provided during wear tear of tools |
Why 4 | Offset Interlock not Available on CNC machine |
Why 5 | |
Root Cause (Occurance) | excess offset provided after re-setting of wear tear tools |
Root Cause Analysis (Outflow)
Why 1 | Defected parts Skipped to costumer |
Why 2 | Setting not ok part mixed up with OK part While inspection |
Why 3 | set up part handling procedure not available |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Setting part handling procedure not Ava liable |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Offset interlock of 0.02mm provided on CNC machine | Santosh Mokal | 06/12/2023 | Pending | |
Outflow | Set up part handling procedure made & desplayed Training given to operator through OPL | Santosh Mokal | 10/12/2023 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection started in place of sampling inspection. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Manual setting for offset 548_Occurance_Before.xlsx |
Occurance (After) |
Offset Inter lock system Provided in programme 548_Occurance_After.xlsx |
Outflow (Before) |
sampling insp 548_Outflow_Before.xlsx |
Outflow (After) |
100 % insp 548_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Supplier END all CNC Machines |
12. Document Review
Documents | ControlPlan, WISOP, InspCheckSheet |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | No Action updated |