QFR No - 7000944097
Defect Details
NC No. 7000944097
NC Date 12/09/2023
NC Submission Date
Part No. 520PP01902
Part Name WHEEL CLUTCH FINISHED UPGRADE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DAMAGES-HEAVY B/H , DAMAGE HARD SPOT ,CHIP OFF
 
1. Problem Description
Defect Description Heavy Blow Hole observed at Friction face & Lug Face
Detection Stage Receipt
Problem Severity Function
NG Quantity 2640
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
500
1000
1500
Check Qty
0
0
0
500
1000
1500
NG Qty
0
0
0
1
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% SEGERATION DONE AT SUPPLIER END STARTED BLUE IDENTIFICATION DOT MARK ON COMPONENTS
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection
 
4. Process Details
Process / Operation casting
Outsource No
Machine / Cell HPDC 400T
Machine / Cell No. 2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManTraining not given to OperatorTraining Plan and on job training record checked.O
MaterialDegassing FrequencyMelting cum furnace degassing report verified & found ok.O
ToolCooling system of dieCooling system of die found ok conditionO
MachineInjection pressureInjection pressure was not constant for every shotX
ManUnskill operator on machineSkill matrix verified & Found ok.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL INSPECTION
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Heavy Blow Hole observed at Friction Face & Lug Face
Why 2 Injection pressure was not constant for every shot.
Why 3 The accumulator cylinder pressure was not constant.
Why 4 The foam was generated due to the oil and N2 gas mixed up.
Why 5
Root Cause (Occurance) The oil seal of the accumulator piston leaked.
 
Root Cause Analysis (Outflow)
Why 1 Heavy Blow Hole Observed at Friction Face & Lug Face
Why 2 Ok parts & Not ok Parts are mixed at the final stage
Why 3 The tag was not available for the ok bins and not the ok bins.
Why 4
Why 5
Root Cause (Outflow) The tag was not available for the ok bins and not the ok bins.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1 Heat exchanger temperature maintained on lower side and machine temperature maintained between 45° C to 50° C. 2.Heat exchanger tubes & descaling done. 3.Cooling tower unit clean and descaling done.Production Supervisor29/09/202329/09/2023Completed
Outflow1.Defective photos big size of board made and displayed. 2.Defective part handling procedure made in local language and A3 SIZE holding displayed. 3. Eye sequence chart in local language and A3 SIZE holding displayed at final inspection table. 4.Training and awareness given to Inspector. 5.Inspector Licenses implemented 6.Lux level maintained as per standardQuality Engineer29/09/202329/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % visual inspection started with identification Marking
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) The cooling tower unit was not clean and descaling.
550_Occurance_Before.png
Occurance (After) 1. Heat exchanger tube descaling done. 2. Cooling tower unit clean and descaling done.
550_Occurance_After.png
Outflow (Before) identification tag was not available in the final inspection bin.
550_Outflow_Before.jfif
Outflow (After) Awarness Training Provide to Final Inspection Inspector & Parts Loading operator.
550_Outflow_After.jfif
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL ETL COMPONENT
 
12. Document Review
Documents InspCheckSheet
Specify Other Document QA OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Ok