QFR No - 7000984362
Defect Details
NC No. 7000984362
NC Date 10/02/2024
NC Submission Date
Part No. F1FA01333M
Part Name FORK PIPE MACHINED-K86A
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details RUSTY-Rust material
 
1. Problem Description
Defect Description Rusty Fork Pipe OD
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 472
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID girisha@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2500
0
0
1000
8200
11700
Check Qty
2500
0
0
1000
8200
11700
NG Qty
472
0
0
23
2900
3395
 
Scrap 0
Rework 3395
Under Deviation 0
Containment Action
100% visual inspection done for Rust on Machined Area at customer end & In- House end.
 
3. Process Flow
Process Flow Description
RM - CNC MACHINING - DRILLING - DEBURRING - FINAL INSPECTION - BIN PACKING - DISPATCH.
 
4. Process Details
Process / Operation CNC MACHINING & INSPECTION
Outsource No
Machine / Cell CNC MACHINING
Machine / Cell No. CELL NO - 5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRM in rusty ConditionVerified the Inward Records & no Rusty RM Reciept evidentX
MachineCoolant Concentration % not AdhequeteCoolant Concentration % cheched & found not Wthin SpecificationO
ManOperator SkillVerified & observed skilled operatoer availibilityX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Sampleplan
7. Root Cause Analysis (Occurance)
Why 1 Fork pipe OD observed Rusty
Why 2 Coolant Concentration %, not Adhequete
Why 3 Coolant Concentration % preparation done by using the wrong inspection method
Why 4 Lack of awareness regarding the use of Refactrometer
Why 5
Root Cause (Occurance) Lack of awareness regarding the use of Refactrometer.
 
Root Cause Analysis (Outflow)
Why 1 Fork pipe OD observed Rusty
Why 2 Not detected during the Final Inspection
Why 3 Lack of awareness to the final inspector regarding the rust issue in the machined tubes supplies
Why 4
Why 5
Root Cause (Outflow) Lack of awareness to the final inspector regarding the rust issue in the machined tube supplies
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowArabian rust Coat RPO Oil application startedMr. Palak Shah08/03/202408/03/2024Completed
OutflowAwareness training given to the final inspector regarding the rust issue in the machined tube suppliesMr. Anaand Nagare10/03/202408/03/2024Completed
OccuranceAuthorized person for coolant prepation identified & Supervisory level approval definedMr. Omkar Wagale10/03/202408/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % Inspection to be done for the rusty Issue
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No Authorized person for coolant preparation was identified & No Supervisory-level approval was defined
675_Occurance_Before.pdf
Occurance (After) Authorized person for coolant prepation identified & Supervisory level approval defined
675_Occurance_After.pdf
Outflow (Before) No Awareness to the final inspector regarding the rust issue in the machined tube supplies & WI for RPO Application
675_Outflow_Before.pdf
Outflow (After) Awareness training given to the final inspector regarding the rust issue in the machined tube supplies
675_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant K0PG
 
12. Document Review
Documents WISOP
Specify Other Document WI & Authorization
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Rust problem in fork pipe K0PG