QFR No - 7000984362
Defect Details
NC No. | 7000984362 |
NC Date | 10/02/2024 |
NC Submission Date | |
Part No. | F1FA01333M |
Part Name | FORK PIPE MACHINED-K86A |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | RUSTY-Rust material |
1. Problem Description
Defect Description | Rusty Fork Pipe OD |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 472 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2500
|
0
|
0
|
1000
|
8200
|
11700
|
Check Qty |
2500
|
0
|
0
|
1000
|
8200
|
11700
|
NG Qty |
472
|
0
|
0
|
23
|
2900
|
3395
|
Scrap | 0 |
Rework | 3395 |
Under Deviation | 0 |
Containment Action |
---|
100% visual inspection done for Rust on Machined Area at customer end & In- House end. |
3. Process Flow
Process Flow Description |
---|
RM - CNC MACHINING - DRILLING - DEBURRING - FINAL INSPECTION - BIN PACKING - DISPATCH. |
4. Process Details
Process / Operation | CNC MACHINING & INSPECTION |
Outsource | No |
Machine / Cell | CNC MACHINING |
Machine / Cell No. | CELL NO - 5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | RM in rusty Condition | Verified the Inward Records & no Rusty RM Reciept evident | X |
Machine | Coolant Concentration % not Adhequete | Coolant Concentration % cheched & found not Wthin Specification | O |
Man | Operator Skill | Verified & observed skilled operatoer availibility | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | Sampleplan |
7. Root Cause Analysis (Occurance)
Why 1 | Fork pipe OD observed Rusty |
Why 2 | Coolant Concentration %, not Adhequete |
Why 3 | Coolant Concentration % preparation done by using the wrong inspection method |
Why 4 | Lack of awareness regarding the use of Refactrometer |
Why 5 | |
Root Cause (Occurance) | Lack of awareness regarding the use of Refactrometer. |
Root Cause Analysis (Outflow)
Why 1 | Fork pipe OD observed Rusty |
Why 2 | Not detected during the Final Inspection |
Why 3 | Lack of awareness to the final inspector regarding the rust issue in the machined tubes supplies |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Lack of awareness to the final inspector regarding the rust issue in the machined tube supplies |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Arabian rust Coat RPO Oil application started | Mr. Palak Shah | 08/03/2024 | 08/03/2024 | Completed |
Outflow | Awareness training given to the final inspector regarding the rust issue in the machined tube supplies | Mr. Anaand Nagare | 10/03/2024 | 08/03/2024 | Completed |
Occurance | Authorized person for coolant prepation identified & Supervisory level approval defined | Mr. Omkar Wagale | 10/03/2024 | 08/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % Inspection to be done for the rusty Issue |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No Authorized person for coolant preparation was identified & No Supervisory-level approval was defined 675_Occurance_Before.pdf |
Occurance (After) |
Authorized person for coolant prepation identified & Supervisory level approval defined 675_Occurance_After.pdf |
Outflow (Before) |
No Awareness to the final inspector regarding the rust issue in the machined tube supplies & WI for RPO Application 675_Outflow_Before.pdf |
Outflow (After) |
Awareness training given to the final inspector regarding the rust issue in the machined tube supplies 675_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | K0PG |
12. Document Review
Documents | WISOP |
Specify Other Document | WI & Authorization |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Rust problem in fork pipe K0PG |