QFR No - 7000985442
Defect Details
NC No. 7000985442
NC Date 14/02/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details HOLE BLOCK-1.50 hole Problem
 
1. Problem Description
Defect Description Hole block 1.50mm in Fork Pipe K0PG
Detection Stage Receipt
Problem Severity Function
NG Quantity 170
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID girisha@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
1300
500
4800
Check Qty
3000
0
0
1300
500
4800
NG Qty
170
0
0
0
0
170
 
Scrap 0
Rework 170
Under Deviation 0
Containment Action
100% inspection done for Drill Hole 1.50 mm with Pin Gauge at customer end & In-house stock available.
 
3. Process Flow
Process Flow Description
RM - CNC MACHINING - DRILLING - DEBURRING - INSPECTION - BIN PACKING - DISPATCH.
 
4. Process Details
Process / Operation DRILLING
Outsource No
Machine / Cell DRILLING MACHINE
Machine / Cell No. DRILL MACHINE - 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolDrill hole burr not cleanedVerifed & found drill hole burr not getting removed from drill hole IDX
MethodDeburring operation not doneVerified & observed deburring operation being doneO
Manunskilled manpowerVerified record & found SkilledO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Deburring Process
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 HOLE BLOCK-1.50 hole Problem
Why 2 Drill hole burr does not get removed in a deburring operation
Why 3 generation of an excess hard burr at hole ID
Why 4 Drill warn out before defined frequency of drill change
Why 5 Drill bit Manufacturing defect
Root Cause (Occurance) Drill bit Manufacturing defect
 
Root Cause Analysis (Outflow)
Why 1 HOLE BLOCK-1.50 hole Problem
Why 2 Drill hole burr does not get removed in a deburring operation
Why 3 Drill hole burr not getting detected in Visual inspection
Why 4 No Inspection Specified in the final Inspection Quality plan for the drill hole block
Why 5
Root Cause (Outflow) No Inspection Specified in the final Inspection Quality plan for the drill hole block
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurancecheck point added in Hourly inspection report for Drill hole blockMr. Abhishek Yadav10/03/202408/03/2024Completed
OutflowInspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per samplinug planMr. Abhishek Yadav10/03/202408/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per samplinug plan
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Sampleplan
10. Evidance of Countermeasure
Occurance (Before) No checkpoint added in Hourly inspection report for Drill hole block
677_Occurance_Before.pdf
Occurance (After) checkpoint added in Hourly inspection report for Drill hole block
677_Occurance_After.pdf
Outflow (Before) No Inspection was Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per the sampling plan
677_Outflow_Before.pdf
Outflow (After) Inspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per sampling plan
677_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant K86
 
12. Document Review
Documents InspCheckSheet
Specify Other Document Quality Plan
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Hole block 1.5 mm in fork pipe K0PG.