QFR No - 7000985442
Defect Details
NC No. | 7000985442 |
NC Date | 14/02/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | HOLE BLOCK-1.50 hole Problem |
1. Problem Description
Defect Description | Hole block 1.50mm in Fork Pipe K0PG |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 170 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
1300
|
500
|
4800
|
Check Qty |
3000
|
0
|
0
|
1300
|
500
|
4800
|
NG Qty |
170
|
0
|
0
|
0
|
0
|
170
|
Scrap | 0 |
Rework | 170 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection done for Drill Hole 1.50 mm with Pin Gauge at customer end & In-house stock available. |
3. Process Flow
Process Flow Description |
---|
RM - CNC MACHINING - DRILLING - DEBURRING - INSPECTION - BIN PACKING - DISPATCH. |
4. Process Details
Process / Operation | DRILLING |
Outsource | No |
Machine / Cell | DRILLING MACHINE |
Machine / Cell No. | DRILL MACHINE - 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Drill hole burr not cleaned | Verifed & found drill hole burr not getting removed from drill hole ID | X |
Method | Deburring operation not done | Verified & observed deburring operation being done | O |
Man | unskilled manpower | Verified record & found Skilled | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Deburring Process |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | HOLE BLOCK-1.50 hole Problem |
Why 2 | Drill hole burr does not get removed in a deburring operation |
Why 3 | generation of an excess hard burr at hole ID |
Why 4 | Drill warn out before defined frequency of drill change |
Why 5 | Drill bit Manufacturing defect |
Root Cause (Occurance) | Drill bit Manufacturing defect |
Root Cause Analysis (Outflow)
Why 1 | HOLE BLOCK-1.50 hole Problem |
Why 2 | Drill hole burr does not get removed in a deburring operation |
Why 3 | Drill hole burr not getting detected in Visual inspection |
Why 4 | No Inspection Specified in the final Inspection Quality plan for the drill hole block |
Why 5 | |
Root Cause (Outflow) | No Inspection Specified in the final Inspection Quality plan for the drill hole block |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | check point added in Hourly inspection report for Drill hole block | Mr. Abhishek Yadav | 10/03/2024 | 08/03/2024 | Completed |
Outflow | Inspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per samplinug plan | Mr. Abhishek Yadav | 10/03/2024 | 08/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per samplinug plan |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | Sampleplan |
10. Evidance of Countermeasure
Occurance (Before) |
No checkpoint added in Hourly inspection report for Drill hole block 677_Occurance_Before.pdf |
Occurance (After) |
checkpoint added in Hourly inspection report for Drill hole block 677_Occurance_After.pdf |
Outflow (Before) |
No Inspection was Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per the sampling plan 677_Outflow_Before.pdf |
Outflow (After) |
Inspection Specified in the final Inspection Quality plan for the drill hole block by using Pin gauge as per sampling plan 677_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | K86 |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | Quality Plan |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Hole block 1.5 mm in fork pipe K0PG. |