QFR No - 7000991752
Defect Details
NC No. 7000991752
NC Date 02/03/2024
NC Submission Date
Part No. 520DZ00212
Part Name FORK BOLT K60-(DS181012)
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1126-ETL Pantnagar
Defect Details SALT SPRAY TEST FAIL-Plating Peel - Off SST fail in 24 Hours
 
1. Problem Description
Defect Description Plating Peel - Off SST fail in 24 Hours
Detection Stage Receipt
Problem Severity Function
NG Quantity 2000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
0
0
2000
Check Qty
2000
0
0
0
0
2000
NG Qty
2000
0
0
0
0
2000
 
Scrap 0
Rework 2000
Under Deviation 0
Containment Action
100% LOT VERIFICATION BY SST AND PLATED PART MOVED IN CURING AREA AFTER PLATING
 
3. Process Flow
Process Flow Description
1-R/M 2-TRUAB OPERATION 3-PUNCHING ,4-TRG GRINDING 5-ROLLING ,6-PLATING 7-FINAL INSPECTION , 8 FINAL INSPECTION 9-PACKING
 
4. Process Details
Process / Operation PLATING
Outsource No
Machine / Cell PLATING
Machine / Cell No. TANK NO-05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRM GRADE AND SIZE NOT OKVALIDATION ANF FOUND OKO
MethodLOT WISE SST NOT CHECKEDVALIDATION ANF FOUND NOT OKX
ManUNAWARENESS OF OPERATORVALIDATION AND FOUND OPERATOR SKILL LEVEL OKO
ToolN/AN/AO
MachineMACHINE TANK NOT CLEAN AS PER PLANVALIDATION AND FOUND NOT OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method SST METHOD
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size As samp
7. Root Cause Analysis (Occurance)
Why 1 SALT SPRAY TEST FAIL-Plating Peel - Off SST fail in 24 Hours
Why 2 CLEANING NOT PROPERLY DONE
Why 3 IN ANODIC CLEANING CURRENT NOT FLOWING PROPERLY.
Why 4 CONTACT POINT FOUND LOOSE .THEREFORE, PROPER CURRENT NOT GET TO PARTS.
Why 5 SCHEDULE MADE FOR ALL CONTACT POINT TO BE CHECK ON WEEKLY BASIS.
Root Cause (Occurance) IN ANODIC CLEANING CURRENT NOT FLOWING PROPERLY. DUE TO LOOSE CONTACT POINT . THEREFORE, PROPER CURRENT NOT GET TO COMPONENTS SO CLEANING WAS NOT PROPER. .
 
Root Cause Analysis (Outflow)
Why 1 SALT SPRAY TEST FAIL-Plating Peel - Off SST fail in 24 Hours
Why 2 LOT WISE SST PLAN NOT PREPARED
Why 3 AS PER PLAN SST NOT DONE LOT WISE
Why 4
Why 5
Root Cause (Outflow) SST PLAN LOT WISE NOT PREPARED
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCLEANING NOT PROPERLY DONEGANESH MAURYA20/03/202419/03/2024Completed
OutflowLOT WISE SST PLAN PREPARED CHECK SHEETMr GANESH MAURYA20/03/202419/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details SST CHECKING PLAN NOT EFFECTIVE
Inspection Method Other
Other Inspection Method SST REPORT
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size LOT WISE
10. Evidance of Countermeasure
Occurance (Before) SALT TEST REPORT UPDATE
708_Occurance_Before.pdf
Occurance (After) PLATING THIKNESS REPORT UPDATE
708_Occurance_After.pdf
Outflow (Before) SST PLAN NOT EFFECTIVE
708_Outflow_Before.xlsx
Outflow (After) LOT WISE SST REPORT PREPARED
708_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant ALL PLATING PART
 
12. Document Review
Documents InspCheckSheet
Specify Other Document SST PLAN UPDATE
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission SST requirement is 168hrs for White Rust & 480hrs for Red Rust, But the plan which you have attached the Red Rust hours mentioned as 400hrs. Secondly Third Party SST Testing done for only 240hrs. Third as the Frequency of your SST is 6 months, then what will be the method to ensure Plating is OK or Not of each lot.