QFR No - 7001001044
Defect Details
NC No. | 7001001044 |
NC Date | 28/03/2024 |
NC Submission Date | |
Part No. | 53BKZ00102 |
Part Name | RUBBER BUSH |
Supplier Name & Code | 101023-FORES ELASTOMECH INDIA PVT. LT |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | DIMETER UNDERSIZE-OD undersize |
1. Problem Description
Defect Description | OD 24.3+0.3/-0.3 observed undersize 23.70 mm. |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 17500 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | malani.pritam@foresgroup.com |
Plant Head/CEO Email ID | singh.barinder@foresgroup.com |
MD Email ID | swamy.pj@foresgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
17500
|
40000
|
0
|
0
|
0
|
57500
|
Check Qty |
17500
|
40000
|
0
|
0
|
0
|
57500
|
NG Qty |
10
|
0
|
0
|
0
|
0
|
10
|
Scrap | 9 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % sorting of Fores stock |
3. Process Flow
Process Flow Description |
---|
Material inward then forward to mixing department after that forward to molding process after that final inspection to standard packing. |
4. Process Details
Process / Operation | Moulding |
Outsource | No |
Machine / Cell | Hyd 250 T |
Machine / Cell No. | 250 T |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | buffing process | Buffing process at parting line | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Venier |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
7. Root Cause Analysis (Occurance)
Why 1 | OD undersize |
Why 2 | OD undersize on parting line |
Why 3 | undersize at parting line de-flash portion |
Why 4 | OD undersize due to buffing process at parting line |
Why 5 | |
Root Cause (Occurance) | OD undersize due to buffing process at parting line |
Root Cause Analysis (Outflow)
Why 1 | OD undersize |
Why 2 | Skipped from Inspection |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Skipped from Inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Buffing process removed. | Fores | 10/04/2024 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Training given to Inspector & OPL displayed. |
Inspection Method | Other |
Other Inspection Method | vernier |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
10. Evidance of Countermeasure
Occurance (Before) |
Parting line De-flashing by buffing wheel 728_Occurance_Before.jpg |
Occurance (After) |
De-flashing process removed. 728_Occurance_After.jpg |
Outflow (Before) |
OD inspection at sampling basis 728_Outflow_Before.jpg |
Outflow (After) |
OD inspection at sampling basis, Sampling Quantity increase. 728_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Rubber bush |
12. Document Review
Documents | |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |