QFR No - 7001013621
Defect Details
NC No. | 7001013621 |
NC Date | 14/05/2024 |
NC Submission Date | |
Part No. | S2CW00612B |
Part Name | D NUT- HF DELUX |
Supplier Name & Code | 100151-EXCELL PRESSINGS |
ETL Plant | 1143-ETL Suspension Halol, Vadodara |
Defect Details | NOT AS PER SPECIFICATION-perpendicularity 0.66 mm against 0.25 mm |
1. Problem Description
Defect Description | Not as per Specification Perpendicularity 0.66 mm against 0.25 mm. |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 4000 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | excellpressings.qc@gmail.com |
Plant Head/CEO Email ID | yogesh_vaidya42@yahoo.co.in |
MD Email ID | excellpressings@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4000
|
0
|
0
|
2000
|
3000
|
9000
|
Check Qty |
4000
|
0
|
0
|
2000
|
3000
|
9000
|
NG Qty |
4000
|
0
|
0
|
1200
|
800
|
6000
|
Scrap | 6000 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
We have checked all the lots available in Finished goods area and parts available in Work in progress, in which some parts are found NG, that will be scraped. |
3. Process Flow
Process Flow Description |
---|
Shearing -Blanking & piercing - ID chamfer- tapping to ID(M9X1.25 6G)-plating-final inspection- dispatch |
4. Process Details
Process / Operation | Tapping opeartion |
Outsource | No |
Machine / Cell | Tapping machine upto M12 |
Machine / Cell No. | EP-25 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | STOPPER STRIP WEAR OUT | STOPPER STRIP FOUND WEAR OUT | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Perpendicularity increased |
Why 2 | Threading has gone crossed while tapping |
Why 3 | Part has moved with tap to upper side,part got tilt by 0.3 mm. |
Why 4 | Stopper strip provided on tapping fixture has wear out |
Why 5 | Not checked the stopper strip |
Root Cause (Occurance) | As the stopper strip was wear out, part came on top side and part get tilted, so perpendicularity increased. |
Root Cause Analysis (Outflow)
Why 1 | Part not checked for perpendicularity |
Why 2 | not aware of problem raised due to perpendicularity |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Perpendicularity was not checked in process and final inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | part will be checked in process inspection and in final inspection for perpendicularity | Ankosh Mathure | 18/05/2024 | 18/05/2024 | Completed |
Occurance | stopper strip will be changed | Ankosh Mathure | 18/05/2024 | 18/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | perpendicularity will be checked for every lot |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
10. Evidance of Countermeasure
Occurance (Before) |
STOPPER STRIP ON TAPPING FIXTURE WEAR OT 802_Occurance_Before.jpg |
Occurance (After) |
NEW STOPPER STRIP OF HARDENED MATERIAL USED 802_Occurance_After.jpg |
Outflow (Before) |
PERPENDICULARITY FOUND NOT OK 802_Outflow_Before.jpg |
Outflow (After) |
PERPENDICULARITY OBSERVED OK 802_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | TAPPING MACHINE EP-17 |
12. Document Review
Documents | PMCheckSheet, InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |