QFR No - 7001013621
Defect Details
NC No. 7001013621
NC Date 14/05/2024
NC Submission Date
Part No. S2CW00612B
Part Name D NUT- HF DELUX
Supplier Name & Code 100151-EXCELL PRESSINGS
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details NOT AS PER SPECIFICATION-perpendicularity 0.66 mm against 0.25 mm
 
1. Problem Description
Defect Description Not as per Specification Perpendicularity 0.66 mm against 0.25 mm.
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID excellpressings.qc@gmail.com
Plant Head/CEO Email ID yogesh_vaidya42@yahoo.co.in
MD Email ID excellpressings@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4000
0
0
2000
3000
9000
Check Qty
4000
0
0
2000
3000
9000
NG Qty
4000
0
0
1200
800
6000
 
Scrap 6000
Rework 0
Under Deviation 0
Containment Action
We have checked all the lots available in Finished goods area and parts available in Work in progress, in which some parts are found NG, that will be scraped.
 
3. Process Flow
Process Flow Description
Shearing -Blanking & piercing - ID chamfer- tapping to ID(M9X1.25 6G)-plating-final inspection- dispatch
 
4. Process Details
Process / Operation Tapping opeartion
Outsource No
Machine / Cell Tapping machine upto M12
Machine / Cell No. EP-25
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolSTOPPER STRIP WEAR OUTSTOPPER STRIP FOUND WEAR OUTO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Perpendicularity increased
Why 2 Threading has gone crossed while tapping
Why 3 Part has moved with tap to upper side,part got tilt by 0.3 mm.
Why 4 Stopper strip provided on tapping fixture has wear out
Why 5 Not checked the stopper strip
Root Cause (Occurance) As the stopper strip was wear out, part came on top side and part get tilted, so perpendicularity increased.
 
Root Cause Analysis (Outflow)
Why 1 Part not checked for perpendicularity
Why 2 not aware of problem raised due to perpendicularity
Why 3
Why 4
Why 5
Root Cause (Outflow) Perpendicularity was not checked in process and final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflowpart will be checked in process inspection and in final inspection for perpendicularityAnkosh Mathure18/05/202418/05/2024Completed
Occurancestopper strip will be changedAnkosh Mathure18/05/202418/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details perpendicularity will be checked for every lot
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) STOPPER STRIP ON TAPPING FIXTURE WEAR OT
802_Occurance_Before.jpg
Occurance (After) NEW STOPPER STRIP OF HARDENED MATERIAL USED
802_Occurance_After.jpg
Outflow (Before) PERPENDICULARITY FOUND NOT OK
802_Outflow_Before.jpg
Outflow (After) PERPENDICULARITY OBSERVED OK
802_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant TAPPING MACHINE EP-17
 
12. Document Review
Documents PMCheckSheet, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission