QFR No - 7001018209
Defect Details
NC No. | 7001018209 |
NC Date | 29/05/2024 |
NC Submission Date | |
Part No. | 520FN04002 |
Part Name | HOLDER CLUTCH |
Supplier Name & Code | 101138-HINDUSTAN PRESSINGS PVT.LTD. |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | DIMN.O/SIZE.-dimn 2.96 ~3.14 u/s & o/s against 3+0.1 |
1. Problem Description
Defect Description | Bearing Resting Height found undersize & Oversize up to 2.96~3.14 mm against 3±0.1 |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 300 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality.p1@hpplindia.com |
Plant Head/CEO Email ID | spatil@hpplindia.com |
MD Email ID | rakesh@hpplindia.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
300
|
0
|
0
|
0
|
500
|
800
|
Check Qty |
300
|
0
|
0
|
0
|
500
|
800
|
NG Qty |
300
|
0
|
0
|
0
|
0
|
300
|
Scrap | 0 |
Rework | 300 |
Under Deviation | 0 |
Containment Action |
---|
Visit to customer end and witness the quality issue. |
3. Process Flow
Process Flow Description |
---|
1)Blaking And piercing 2)Sandering 3)Chamfer 4)machining 5)Final inspection and packeging 6)PDIR and Dispatch |
4. Process Details
Process / Operation | Machining |
Outsource | Yes |
Machine / Cell | CNC machine |
Machine / Cell No. | Machine no-1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | THICKNESS VARIATION MAY CAUSE HEIGHT ISSUE DURING MACHING STAGE | 100% GAP GAUGE SHOULD BE DONE TO SEGRIGATE THE PARTS, ACCODING TO THCKINESS, WHICH HELPS TO MACHININ | X |
Tool | DAMAGED TOOL USED | TOOL CONDITION WAS OK. | O |
Machine | MACHINING NOT DONE PROPERLY | MACHINING DONE PROPERLY | O |
Man | POOR MATERIAL HANDLING&DURING INPROCESS, INSPECTION. | THERE WAS NO PROPER METHOD TO CHECK PART THICKNESS INDIDUALLY | X |
Method | RAW MATERIAL THICKNESS USED TO CHECK AT SAMPLE BASIS AT RECEIVING STAGE | AFTER BLANKING STAGE VARIATION IN THICKNESS THAT WAS UNDER TOLERENCE | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Thickness variation in part is causing height issue at machining stage. |
Why 2 | height dimension checking being done on sample basis. |
Why 3 | gap gauge was not using for to identify thckiness variation parts. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Due to thickness variation in parts causing height issue at maching stage |
Root Cause Analysis (Outflow)
Why 1 | Bearing Resting Height found undersize & Oversize up to 2.96~3.14 mm against 3±0.1 |
Why 2 | Defect found at ETL at recipt stage. |
Why 3 | defect causing fitment issue at assembly line |
Why 4 | Sample basis inspection done by final inspector but defect not detected. |
Why 5 | less awareness to inspector regarding depth checking with dail gauge. |
Root Cause (Outflow) | less awareness to inspector regarding height issue and how to check properly. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Before sending to machining 100 % gap gauge is must done. So that we can seggrigate thickness variation parts to avoid further height issue.. | Mr. Hitendra Patil and Mr, Ningaraj S | 21/06/2024 | 21/06/2024 | Completed |
Occurance | Awareness given to the inspectors regarding height issue. | Mr.Kiran W | 21/06/2024 | 21/06/2024 | Completed |
Outflow | 1. Training given to inspectors regarding all final inspection activities of 4002 holder,specially focussing on height issue. 2. 100% inspection at HPPL pune from QA person for next 3 lot | Mr.Ningaraj S( HPPL) | 21/06/2024 | 21/06/2024 | Completed |
Occurance | Work instruction of RM checking updated for the thickness variation acceptance. | Mr Kiran | 21/06/2024 | 21/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Before Machining proce we do the gap gauge inspection. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Work instruction of RM inspection. 830_Occurance_Before.pdf |
Occurance (After) |
Work instruction for RM checking to b updated as per the thickness. 830_Occurance_After.pdf |
Outflow (Before) |
We have not implemented the gap gauge for checking. 830_Outflow_Before.pdf |
Outflow (After) |
We check with gap gauge before sending to maching. 830_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | No |
12. Document Review
Documents | ControlPlan, WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | OK |