QFR No - 7001018209
Defect Details
NC No. 7001018209
NC Date 29/05/2024
NC Submission Date
Part No. 520FN04002
Part Name HOLDER CLUTCH
Supplier Name & Code 101138-HINDUSTAN PRESSINGS PVT.LTD.
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DIMN.O/SIZE.-dimn 2.96 ~3.14 u/s & o/s against 3+0.1
 
1. Problem Description
Defect Description Bearing Resting Height found undersize & Oversize up to 2.96~3.14 mm against 3±0.1
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 300
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality.p1@hpplindia.com
Plant Head/CEO Email ID spatil@hpplindia.com
MD Email ID rakesh@hpplindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
300
0
0
0
500
800
Check Qty
300
0
0
0
500
800
NG Qty
300
0
0
0
0
300
 
Scrap 0
Rework 300
Under Deviation 0
Containment Action
Visit to customer end and witness the quality issue.
 
3. Process Flow
Process Flow Description
1)Blaking And piercing 2)Sandering 3)Chamfer 4)machining 5)Final inspection and packeging 6)PDIR and Dispatch
 
4. Process Details
Process / Operation Machining
Outsource Yes
Machine / Cell CNC machine
Machine / Cell No. Machine no-1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialTHICKNESS VARIATION MAY CAUSE HEIGHT ISSUE DURING MACHING STAGE100% GAP GAUGE SHOULD BE DONE TO SEGRIGATE THE PARTS, ACCODING TO THCKINESS, WHICH HELPS TO MACHININX
ToolDAMAGED TOOL USEDTOOL CONDITION WAS OK.O
MachineMACHINING NOT DONE PROPERLYMACHINING DONE PROPERLYO
ManPOOR MATERIAL HANDLING&DURING INPROCESS, INSPECTION.THERE WAS NO PROPER METHOD TO CHECK PART THICKNESS INDIDUALLYX
MethodRAW MATERIAL THICKNESS USED TO CHECK AT SAMPLE BASIS AT RECEIVING STAGEAFTER BLANKING STAGE VARIATION IN THICKNESS THAT WAS UNDER TOLERENCEO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Thickness variation in part is causing height issue at machining stage.
Why 2 height dimension checking being done on sample basis.
Why 3 gap gauge was not using for to identify thckiness variation parts.
Why 4
Why 5
Root Cause (Occurance) Due to thickness variation in parts causing height issue at maching stage
 
Root Cause Analysis (Outflow)
Why 1 Bearing Resting Height found undersize & Oversize up to 2.96~3.14 mm against 3±0.1
Why 2 Defect found at ETL at recipt stage.
Why 3 defect causing fitment issue at assembly line
Why 4 Sample basis inspection done by final inspector but defect not detected.
Why 5 less awareness to inspector regarding depth checking with dail gauge.
Root Cause (Outflow) less awareness to inspector regarding height issue and how to check properly.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceBefore sending to machining 100 % gap gauge is must done. So that we can seggrigate thickness variation parts to avoid further height issue..Mr. Hitendra Patil and Mr, Ningaraj S21/06/202421/06/2024Completed
OccuranceAwareness given to the inspectors regarding height issue.Mr.Kiran W21/06/202421/06/2024Completed
Outflow1. Training given to inspectors regarding all final inspection activities of 4002 holder,specially focussing on height issue. 2. 100% inspection at HPPL pune from QA person for next 3 lotMr.Ningaraj S( HPPL)21/06/202421/06/2024Completed
OccuranceWork instruction of RM checking updated for the thickness variation acceptance.Mr Kiran21/06/202421/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Before Machining proce we do the gap gauge inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Work instruction of RM inspection.
830_Occurance_Before.pdf
Occurance (After) Work instruction for RM checking to b updated as per the thickness.
830_Occurance_After.pdf
Outflow (Before) We have not implemented the gap gauge for checking.
830_Outflow_Before.pdf
Outflow (After) We check with gap gauge before sending to maching.
830_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission OK