QFR No - 7001036040
Defect Details
NC No. | 7001036040 |
NC Date | 23/07/2024 |
NC Submission Date | |
Part No. | B2EH08602O |
Part Name | END CONNECTOR CALIPER SIDE N-TORQ |
Supplier Name & Code | 101221-SUNREN AUTOMOTIVE PRIVATE LIMI |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | DENTS & DAMAGES-DENTS & DAMAGES |
1. Problem Description
Defect Description | DENTS & DAMAGES-DENTS & DAMAGES |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 318 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | shivank@sunren.in |
Plant Head/CEO Email ID | sanjayrana@sunren.in |
MD Email ID | subhashsaini@sunren.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6000
|
9000
|
2500
|
1000
|
8000
|
26500
|
Check Qty |
6000
|
9000
|
2500
|
1000
|
8000
|
26500
|
NG Qty |
318
|
120
|
65
|
0
|
0
|
503
|
Scrap | 0 |
Rework | 503 |
Under Deviation | 0 |
Containment Action |
---|
Re-Inspection For All The Suspected Qty. |
3. Process Flow
Process Flow Description |
---|
Forging-Centerless Grinding-1st Cutting-2nd Cutting-Milling-Cross Drill-Facing 1st- Facing 2nd -Neck Drill-Cross Reamer-Chamfer-Air Cleaning-Pin Tray-Visual Inspection-Bending-Identification Marking-Plating-Final Inspection-Dispatch. |
4. Process Details
Process / Operation | Centerless Grinding ,Milling, Cross Drill, |
Outsource | No |
Machine / Cell | 01 |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Wrong Method | Appropriate Method Not Followed | O |
Man | Lack Of Awareness | Not Aware | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Due to poor handling |
Why 2 | Material Handling Method Not Followed |
Why 3 | Lack of Awareness |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Material to Material Contact due to the poor handling. |
Root Cause Analysis (Outflow)
Why 1 | Due to visual detection only. |
Why 2 | Inspector was not aware. |
Why 3 | Due to lack of Training |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Lack of Defect Awareness Training |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Material Handling Training Will be provided to the operators. | Amit | 01/08/2024 | 01/08/2024 | Completed |
Outflow | Defect Awareness Training given to the inspectors. | Amit | 01/08/2024 | 01/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspectors will check the material as per the defect matrix. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
10. Evidance of Countermeasure
Occurance (Before) |
Poor Handling 957_Occurance_Before.jpg |
Occurance (After) |
Material Handling Training Provided to the operators. 957_Occurance_After.pdf |
Outflow (Before) |
Lack of Awareness Training 957_Outflow_Before.jpg |
Outflow (After) |
Awareness training provided to the inspectors. 957_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Parts |
12. Document Review
Documents | |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | found ok |