QFR No - 7001045399
Defect Details
NC No. 7001045399
NC Date 21/08/2024
NC Submission Date
Part No. F2DZ08810B
Part Name K0PG FORK BOLT
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1136-ETL Suspension Sanand
Defect Details PLATING NOT OK-Plating milky white ,black spot
 
1. Problem Description
Defect Description Plating defect i.e. milky white and Black spot .
Detection Stage Inprocess
Problem Severity Function
NG Quantity 721
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7200
9800
0
5000
0
22000
Check Qty
7200
9800
0
5000
0
22000
NG Qty
780
10
0
0
0
790
 
Scrap 0
Rework 780
Under Deviation 0
Containment Action
All pipeline material segregated at customer end, warehouse and FG stock
 
3. Process Flow
Process Flow Description
Incoming RM-Parting-CNC 1st-CNC 2nd-Plating-Final Inspection-PDI-Packing and forwarding
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell Plating cell
Machine / Cell No. Plating cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineProcess Parameter wrongFound as per control planO
MethodJig not clean properlyCleaned properly at defined frequencyO
MethodPart not Loaded properlyPart loaded properly as per SOPO
MethodCuring Time not givenCuring not doneX
MethodInspection frequencyInspection frequency lessX
ToolTool changeNo changeO
MaterialPH variationPH found OKO
MachineTank not discardedfound okO
ManNew manpowerManpower not changedO
MaterialIncorrect ChemicalFound okO
ManUnskilled OperatorSkill manpower available as per skill matrixO
MaterialVariation in ChemicalChemical found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 nos
7. Root Cause Analysis (Occurance)
Why 1 Plating Not ok
Why 2 Found Rusty, black spot
Why 3 Part dispatched without curing process
Why 4
Why 5
Root Cause (Occurance) Curing process not done
 
Root Cause Analysis (Outflow)
Why 1 Plating Not ok
Why 2 Found Rusty, black spot
Why 3 Skipped from final inspection stage
Why 4 Inspection frequency is low
Why 5
Root Cause (Outflow) Inspection frequency is low
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOnjob training given to Operator about process awarenessMr. Pradeep Bhagwat16/08/202416/08/2024Completed
OutflowInspection frequency increased from 10nos per lot to 20nos per lotMr. Pradeep bhagwat16/08/202416/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection frequency inscreased
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Curing process SOP not displayed
1029_Occurance_Before.jpg
Occurance (After) Curing process SOP displayd
1029_Occurance_After.jpg
Outflow (Before) Inspection frequency less
1029_Outflow_Before.jpg
Outflow (After) Onjob training given to operator and inspector for defect awareness and inspection frequency 20nos per lot
1029_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Plating cell
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission PLATING NOT OK-Plating milky white ,black spot.