QFR No - 7001045399
Defect Details
NC No. | 7001045399 |
NC Date | 21/08/2024 |
NC Submission Date | |
Part No. | F2DZ08810B |
Part Name | K0PG FORK BOLT |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | PLATING NOT OK-Plating milky white ,black spot |
1. Problem Description
Defect Description | Plating defect i.e. milky white and Black spot . |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 721 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7200
|
9800
|
0
|
5000
|
0
|
22000
|
Check Qty |
7200
|
9800
|
0
|
5000
|
0
|
22000
|
NG Qty |
780
|
10
|
0
|
0
|
0
|
790
|
Scrap | 0 |
Rework | 780 |
Under Deviation | 0 |
Containment Action |
---|
All pipeline material segregated at customer end, warehouse and FG stock |
3. Process Flow
Process Flow Description |
---|
Incoming RM-Parting-CNC 1st-CNC 2nd-Plating-Final Inspection-PDI-Packing and forwarding |
4. Process Details
Process / Operation | Plating |
Outsource | Yes |
Machine / Cell | Plating cell |
Machine / Cell No. | Plating cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Process Parameter wrong | Found as per control plan | O |
Method | Jig not clean properly | Cleaned properly at defined frequency | O |
Method | Part not Loaded properly | Part loaded properly as per SOP | O |
Method | Curing Time not given | Curing not done | X |
Method | Inspection frequency | Inspection frequency less | X |
Tool | Tool change | No change | O |
Material | PH variation | PH found OK | O |
Machine | Tank not discarded | found ok | O |
Man | New manpower | Manpower not changed | O |
Material | Incorrect Chemical | Found ok | O |
Man | Unskilled Operator | Skill manpower available as per skill matrix | O |
Material | Variation in Chemical | Chemical found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Plating Not ok |
Why 2 | Found Rusty, black spot |
Why 3 | Part dispatched without curing process |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Curing process not done |
Root Cause Analysis (Outflow)
Why 1 | Plating Not ok |
Why 2 | Found Rusty, black spot |
Why 3 | Skipped from final inspection stage |
Why 4 | Inspection frequency is low |
Why 5 | |
Root Cause (Outflow) | Inspection frequency is low |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Onjob training given to Operator about process awareness | Mr. Pradeep Bhagwat | 16/08/2024 | 16/08/2024 | Completed |
Outflow | Inspection frequency increased from 10nos per lot to 20nos per lot | Mr. Pradeep bhagwat | 16/08/2024 | 16/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection frequency inscreased |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Curing process SOP not displayed 1029_Occurance_Before.jpg |
Occurance (After) |
Curing process SOP displayd 1029_Occurance_After.jpg |
Outflow (Before) |
Inspection frequency less 1029_Outflow_Before.jpg |
Outflow (After) |
Onjob training given to operator and inspector for defect awareness and inspection frequency 20nos per lot 1029_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Plating cell |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | PLATING NOT OK-Plating milky white ,black spot. |