QFR No - 7001045569
Defect Details
NC No. 7001045569
NC Date 22/08/2024
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details PLATING NOT OK-Plating problem , milky, white rust
 
1. Problem Description
Defect Description Plating defect i.e. White rust.
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 6000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6000
0
0
1200
0
7200
Check Qty
6000
0
0
1200
0
7200
NG Qty
6000
0
0
1200
0
7200
 
Scrap 0
Rework 7200
Under Deviation 0
Containment Action
Re-plating to be done in all parts
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 REROUNDING 120 BROACHING 130 HEAD GRINDING 140 OUTSIDE MOVEMENT FOR PLATING 150 STORAGE & RQC INSP. OF PLATED MATERIAL 160 FINAL INSPECTION 170 PACKING & DISPATCH
 
4. Process Details
Process / Operation 140 OUTSIDE MOVEMENT FOR PLATING
Outsource Yes
Machine / Cell Plating line
Machine / Cell No. Plating Line
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolWrong tank usedFound okX
MaterialWrong chemical usedChemical checked and found okX
MaterialChemical concertation was not okTesting done at internal lab and found okX
MethodTemperature specificationTemperature was 51 against specification 50 to 80O
MachineBath cleaning tank was not workingChecked and found okX
MachineZinc plating tank was not workingChecked and found okX
MethodProcess sequence was wrongProcess and and found as per control planX
MethodSOP not followedSOP followed and records verifiedX
ManUnskilled manpowerSkill matrix availableX
MachineOven was not okOven is working but temperature was lower side of specO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size sampling
7. Root Cause Analysis (Occurance)
Why 1 Plating problem , milky, white rust
Why 2 Passivation colure changed on part surface
Why 3 Some moisture content was available at part surface
Why 4 Part was not properly dry in oven
Why 5 Temperature was in range but lower side because of One heater is not working
Root Cause (Occurance) 1-Some moisture content was available at part surface due to part was not dry 2-Temperature was in range but lower side because of One heater is not working
 
Root Cause Analysis (Outflow)
Why 1 Plating problem , milky, white rust
Why 2 Final inspector not detect the ng part at Final inspection stage
Why 3 Visual inspection was not done properly for shade mismatch
Why 4 Checker was not understand the parts appearance status during visual inspection
Why 5 Low lux level at inspection table
Root Cause (Outflow) Checker was not understand the parts appearance status during visual inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOven preventive maintenance revised and now maintenance will done on weekly basis instead monthlySupplier25/08/202425/08/2024Completed
OccuranceTemperature parameter changed 50 TO 80 and increased temperature 70-80 to prevent the low temperature issue .Supplier25/08/202425/08/2024Completed
OutflowCover holder bulb added at final inspection to increase the lux level .Nice25/08/202425/08/2024Completed
OccuranceLux level monitoring startedSupplier25/08/202425/08/2024Completed
Outflowcuring time increased Now 36 hrs from 24 hrs at Nice endNice24/08/202425/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Curing time incraesed
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) NA
1030_Occurance_Before.png
Occurance (After) LUX LEVEL
1030_Occurance_After.png
Outflow (Before) NA
1030_Outflow_Before.png
Outflow (After) OVEN DAILY CHECKSHEET
1030_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents PMCheckSheet, WISOP, JHCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission