QFR No - 7001045569
Defect Details
NC No. | 7001045569 |
NC Date | 22/08/2024 |
NC Submission Date | |
Part No. | S1AB00612B |
Part Name | ADJUSTER PLATED |
Supplier Name & Code | 100782-NICE STEEL INDUSTRIES |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | PLATING NOT OK-Plating problem , milky, white rust |
1. Problem Description
Defect Description | Plating defect i.e. White rust. |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 6000 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | ppc.nice@batragroup.biz |
Plant Head/CEO Email ID | ho.nice@batragroup.biz |
MD Email ID | hitesh@batragroup.biz |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6000
|
0
|
0
|
1200
|
0
|
7200
|
Check Qty |
6000
|
0
|
0
|
1200
|
0
|
7200
|
NG Qty |
6000
|
0
|
0
|
1200
|
0
|
7200
|
Scrap | 0 |
Rework | 7200 |
Under Deviation | 0 |
Containment Action |
---|
Re-plating to be done in all parts |
3. Process Flow
Process Flow Description |
---|
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 REROUNDING 120 BROACHING 130 HEAD GRINDING 140 OUTSIDE MOVEMENT FOR PLATING 150 STORAGE & RQC INSP. OF PLATED MATERIAL 160 FINAL INSPECTION 170 PACKING & DISPATCH |
4. Process Details
Process / Operation | 140 OUTSIDE MOVEMENT FOR PLATING |
Outsource | Yes |
Machine / Cell | Plating line |
Machine / Cell No. | Plating Line |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Wrong tank used | Found ok | X |
Material | Wrong chemical used | Chemical checked and found ok | X |
Material | Chemical concertation was not ok | Testing done at internal lab and found ok | X |
Method | Temperature specification | Temperature was 51 against specification 50 to 80 | O |
Machine | Bath cleaning tank was not working | Checked and found ok | X |
Machine | Zinc plating tank was not working | Checked and found ok | X |
Method | Process sequence was wrong | Process and and found as per control plan | X |
Method | SOP not followed | SOP followed and records verified | X |
Man | Unskilled manpower | Skill matrix available | X |
Machine | Oven was not ok | Oven is working but temperature was lower side of spec | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | sampling |
7. Root Cause Analysis (Occurance)
Why 1 | Plating problem , milky, white rust |
Why 2 | Passivation colure changed on part surface |
Why 3 | Some moisture content was available at part surface |
Why 4 | Part was not properly dry in oven |
Why 5 | Temperature was in range but lower side because of One heater is not working |
Root Cause (Occurance) | 1-Some moisture content was available at part surface due to part was not dry 2-Temperature was in range but lower side because of One heater is not working |
Root Cause Analysis (Outflow)
Why 1 | Plating problem , milky, white rust |
Why 2 | Final inspector not detect the ng part at Final inspection stage |
Why 3 | Visual inspection was not done properly for shade mismatch |
Why 4 | Checker was not understand the parts appearance status during visual inspection |
Why 5 | Low lux level at inspection table |
Root Cause (Outflow) | Checker was not understand the parts appearance status during visual inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Oven preventive maintenance revised and now maintenance will done on weekly basis instead monthly | Supplier | 25/08/2024 | 25/08/2024 | Completed |
Occurance | Temperature parameter changed 50 TO 80 and increased temperature 70-80 to prevent the low temperature issue . | Supplier | 25/08/2024 | 25/08/2024 | Completed |
Outflow | Cover holder bulb added at final inspection to increase the lux level . | Nice | 25/08/2024 | 25/08/2024 | Completed |
Occurance | Lux level monitoring started | Supplier | 25/08/2024 | 25/08/2024 | Completed |
Outflow | curing time increased Now 36 hrs from 24 hrs at Nice end | Nice | 24/08/2024 | 25/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Curing time incraesed |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
NA 1030_Occurance_Before.png |
Occurance (After) |
LUX LEVEL 1030_Occurance_After.png |
Outflow (Before) |
NA 1030_Outflow_Before.png |
Outflow (After) |
OVEN DAILY CHECKSHEET 1030_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | PMCheckSheet, WISOP, JHCheckSheet |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |