QFR No - 7001049474
Defect Details
NC No. 7001049474
NC Date 02/09/2024
NC Submission Date
Part No. 520HP00212
Part Name OIL SEAL STOPPER1
Supplier Name & Code 100179-BELLITE SPRINGS PVT.LTD.
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIMN.U/SIZE.-Dim 13.5 undersize
 
1. Problem Description
Defect Description Dim 13.5 mm found undersize i.e. 12.644 mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 30000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc.plant2@bellitespring.com
Plant Head/CEO Email ID dayanandkore@bellitesprings.com
MD Email ID harsjeet.bhatt@bellitesprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
53900
0
0
20000
0
73900
Check Qty
53900
0
0
20000
0
73900
NG Qty
30000
0
0
0
0
30000
 
Scrap 0
Rework 30000
Under Deviation 0
Containment Action
Re verify the Existing lot for the issue
 
3. Process Flow
Process Flow Description
RM Inward-Coiling-Stress Relieving-Checking-Packing-Dispatch
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell CNC Coiling
Machine / Cell No. CNC-02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineIncomplete stroke of notching tool.Checked & found not okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Circlip Gap U/S
Why 2 The notch stroke was not completed.
Why 3 the stroke stopper was loose
Why 4 the bolt was loosened
Why 5 the check nut was missing.
Root Cause (Occurance) the check nut was missing.
 
Root Cause Analysis (Outflow)
Why 1 Circlip Gap U/S
Why 2 To address the issue of undersized circlips not being identified during the final inspection stage
Why 3 due to sampling-based checks with the digital vernier caliper.
Why 4
Why 5
Root Cause (Outflow) due to sampling-based checks with the digital vernier caliper.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew Check Nut is use and stopper is tightened.Mr. Sujit M.19/08/202419/08/2024Completed
OutflowWe have started 100% inspection at the final inspection stageMr. Sujit07/09/202407/09/2024Completed
Occurancethe `Nut and Bolt` checkpoint has been added to the process setup approval report..Mr. Sujit M.20/08/202420/08/2024Completed
OutflowThe PDI report has been updated to include the use of the gap gaugeMr. Sujit07/09/202407/09/2024Completed
OccuranceTightening by two check nuts one above the other.Mr. Sujit M.10/09/202410/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details We are now using a gap gauge for checking circlips at the PDI stage
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) Previously, only one bolt was used.
1051_Occurance_Before.jpg
Occurance (After) Now, Tightening by two check nuts one above the other.
1051_Occurance_After.jpg
Outflow (Before) Previously, we checked the circlip using a vernier caliper during the PDI stage
1051_Outflow_Before.xlsx
Outflow (After) We are now using a gap gauge for checking circlips at the PDI stage
1051_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CNC-02
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document Setup Approval
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Dim 13.5 mm found undersize i.e. 12.644 mm