QFR No - 7001055337
Defect Details
NC No. 7001055337
NC Date 19/09/2024
NC Submission Date
Part No. 520AE00400
Part Name CORE PLATE REDUCED 612
Supplier Name & Code 100959-AAR CEE ENGINEERING WORKS UNIT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details NON FILLING-Non Felling ,Blow Hole
 
1. Problem Description
Defect Description Heavy Non filling ,Blow Hole & crack observed
Detection Stage Receipt
Problem Severity Function
NG Quantity 416
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc@aarceeengg.com
Plant Head/CEO Email ID planthead.diecasting@aarceeengg.com
MD Email ID vaibhav.arora@aarceeengg.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
416
5000
10000
0
0
15416
Check Qty
416
5000
10000
0
0
15416
NG Qty
416
0
0
0
0
416
 
Scrap 416
Rework 0
Under Deviation 0
Containment Action
All available stock will be quarantine and seggrigation100%
 
3. Process Flow
Process Flow Description
1)raw material receipt 2)Storage of Raw Material3)Holding Cum Melting 4) PDC 5) 1st trimming 6) Shot Blasting for burr removing 7)Final Inspection & Packing 8) Stress Relieving 9)Sound Testing10)Shot Blasting 11)Barreling12)2nd Trimming
 
4. Process Details
Process / Operation CASTING
Outsource Yes
Machine / Cell HPDC
Machine / Cell No. 7
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodTrapped air in the mold or die cavity.Air entrapmentX
ManImproper InspectionInspection not done properlyX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 125
7. Root Cause Analysis (Occurance)
Why 1 Air entrapment
Why 2 turbulent metal flow
Why 3 inadequate gas removal
Why 4 Dissolved gases in molten metal ( nitrogen)
Why 5 higher temps increase gas solubility
Root Cause (Occurance) higher temps increase gas solubility
 
Root Cause Analysis (Outflow)
Why 1 Blow hole in core plate
Why 2 Human error
Why 3 Lack of attention or focus
Why 4 Lack of training or experience
Why 5
Root Cause (Outflow) Lack of training or experience
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Optimize temperature control. 2.W.I has been updated for temperature control. 3.Training Provided to the Operator. 4)monitor and control casting temperatureANIRUDH/RITIK23/09/202423/09/2024Completed
Occurance1.Regular training and refresher courses 2. Performance monitoring and feedback(poision test) 3.Q-Sustenance monitoring Check sheet has been Implemented. 4. Quality Inspector initial marking done on each & every piece.Nishant22/09/202422/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no
Inspection Method Other
Other Inspection Method visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 125
10. Evidance of Countermeasure
Occurance (Before) Temperature inspection frequency less in process inspection report
1104_Occurance_Before.xls
Occurance (After) 1. Optimize temperature control. 2.Training Provided to the Operator. 3)monitor and control casting temperature
1104_Occurance_After.xls
Outflow (Before) Inadequate inspector performance monitoring
1104_Outflow_Before.xls
Outflow (After) 1.Regular training and refresher courses 2. Performance monitoring and feedback(poision test) 3.Q-Sustenance monitoring Check sheet has been Implemented. 4. Quality Inspector initial marking done on each & every piece.
1104_Outflow_After.xls
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant k70,3w4s
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document dock audit
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission Ok