QFR No - 7001055337
Defect Details
NC No. | 7001055337 |
NC Date | 19/09/2024 |
NC Submission Date | |
Part No. | 520AE00400 |
Part Name | CORE PLATE REDUCED 612 |
Supplier Name & Code | 100959-AAR CEE ENGINEERING WORKS UNIT |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | NON FILLING-Non Felling ,Blow Hole |
1. Problem Description
Defect Description | Heavy Non filling ,Blow Hole & crack observed |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 416 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qc@aarceeengg.com |
Plant Head/CEO Email ID | planthead.diecasting@aarceeengg.com |
MD Email ID | vaibhav.arora@aarceeengg.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
416
|
5000
|
10000
|
0
|
0
|
15416
|
Check Qty |
416
|
5000
|
10000
|
0
|
0
|
15416
|
NG Qty |
416
|
0
|
0
|
0
|
0
|
416
|
Scrap | 416 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All available stock will be quarantine and seggrigation100% |
3. Process Flow
Process Flow Description |
---|
1)raw material receipt 2)Storage of Raw Material3)Holding Cum Melting 4) PDC 5) 1st trimming 6) Shot Blasting for burr removing 7)Final Inspection & Packing 8) Stress Relieving 9)Sound Testing10)Shot Blasting 11)Barreling12)2nd Trimming |
4. Process Details
Process / Operation | CASTING |
Outsource | Yes |
Machine / Cell | HPDC |
Machine / Cell No. | 7 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Trapped air in the mold or die cavity. | Air entrapment | X |
Man | Improper Inspection | Inspection not done properly | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 125 |
7. Root Cause Analysis (Occurance)
Why 1 | Air entrapment |
Why 2 | turbulent metal flow |
Why 3 | inadequate gas removal |
Why 4 | Dissolved gases in molten metal ( nitrogen) |
Why 5 | higher temps increase gas solubility |
Root Cause (Occurance) | higher temps increase gas solubility |
Root Cause Analysis (Outflow)
Why 1 | Blow hole in core plate |
Why 2 | Human error |
Why 3 | Lack of attention or focus |
Why 4 | Lack of training or experience |
Why 5 | |
Root Cause (Outflow) | Lack of training or experience |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1. Optimize temperature control. 2.W.I has been updated for temperature control. 3.Training Provided to the Operator. 4)monitor and control casting temperature | ANIRUDH/RITIK | 23/09/2024 | 23/09/2024 | Completed |
Occurance | 1.Regular training and refresher courses 2. Performance monitoring and feedback(poision test) 3.Q-Sustenance monitoring Check sheet has been Implemented. 4. Quality Inspector initial marking done on each & every piece. | Nishant | 22/09/2024 | 22/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | no |
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 125 |
10. Evidance of Countermeasure
Occurance (Before) |
Temperature inspection frequency less in process inspection report 1104_Occurance_Before.xls |
Occurance (After) |
1. Optimize temperature control.
2.Training Provided to the Operator.
3)monitor and control casting temperature 1104_Occurance_After.xls |
Outflow (Before) |
Inadequate inspector performance monitoring 1104_Outflow_Before.xls |
Outflow (After) |
1.Regular training and refresher courses
2. Performance monitoring and feedback(poision test)
3.Q-Sustenance monitoring Check sheet has been Implemented.
4. Quality Inspector initial marking done on each & every piece. 1104_Outflow_After.xls |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | k70,3w4s |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | dock audit |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | Ok |