QFR No - 7001062399
Defect Details
NC No. 7001062399
NC Date 11/10/2024
NC Submission Date
Part No. S1JL03533B
Part Name PISTON ROD BOTH SIDE MACHINED
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1
 
1. Problem Description
Defect Description LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 14
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
600
0
0
0
0
600
Check Qty
600
0
0
0
0
600
NG Qty
14
0
0
0
0
14
 
Scrap 14
Rework 0
Under Deviation 0
Containment Action
All Material segregation at Customer End
 
3. Process Flow
Process Flow Description
RM inward - store - Band Saw Parting -Straightening - CNC-1( Mounting Side - CNC-2( Piston Side)- Final inspection - Packing - Dispatch - Transport
 
4. Process Details
Process / Operation CNC-2( Piston Side
Outsource Yes
Machine / Cell CNC-9
Machine / Cell No. CNC Section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachining Process & Inspection Method WrongMachining Process is ok But Inspection Method WrongX
ManUnskilled operatorAs per Skilled Matrix Operator is skilledO
ToolWrong Tool Insert UseCorrect carbide Insert Facing and Turning Tool UseO
MaterialWrong Grade And other grade Material UseCorrect Grade F15.4-EN8D Material use .O
MethodMachine Condition Not OKAs per Daily Check sheet Machine Condition was ok but Stopper Not OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20Nos /Bin
7. Root Cause Analysis (Occurance)
Why 1 LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1
Why 2 During piston side machining, the part was resting too deep in the CNC chuck
Why 3 CNC Resting stopper lock Nut Loose
Why 4
Why 5
Root Cause (Occurance) CNC Resting stopper lock Nut Loose.
 
Root Cause Analysis (Outflow)
Why 1 LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1
Why 2 Sampling measuring Frequency Very Low.
Why 3 Hourly 5 Nos Inspection By Inspector.
Why 4
Why 5
Root Cause (Outflow) Sampling measuring Frequency Very Low.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceArrange an additional lock nut to secure the resting stopper lock nut.Production Head14/10/202414/10/2024Completed
OutflowThe length measurement sampling frequency has been increased to 10 samples instead of 5.Quality Head14/10/202414/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Length measurement sampling frequency has been increased to 10nos samples instead of 5.nos
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10Nos
10. Evidance of Countermeasure
Occurance (Before) CNC Resting stopper lock Nut Loose.
1140_Occurance_Before.jpg
Occurance (After) Arrange an additional lock nut to secure the resting stopper lock nut.
1140_Occurance_After.jpg
Outflow (Before) Sampling measuring Frequency Very Low.
1140_Outflow_Before.docx
Outflow (After) The length measurement sampling frequency has been increased to 10Nos samples instead of 5Nos.
1140_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Piston Rods
 
12. Document Review
Documents ControlPlan, PFMEA, JHCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission