QFR No - 7001062399
Defect Details
NC No. | 7001062399 |
NC Date | 11/10/2024 |
NC Submission Date | |
Part No. | S1JL03533B |
Part Name | PISTON ROD BOTH SIDE MACHINED |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1 |
1. Problem Description
Defect Description | LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 14 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
600
|
0
|
0
|
0
|
0
|
600
|
Check Qty |
600
|
0
|
0
|
0
|
0
|
600
|
NG Qty |
14
|
0
|
0
|
0
|
0
|
14
|
Scrap | 14 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Material segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
RM inward - store - Band Saw Parting -Straightening - CNC-1( Mounting Side - CNC-2( Piston Side)- Final inspection - Packing - Dispatch - Transport |
4. Process Details
Process / Operation | CNC-2( Piston Side |
Outsource | Yes |
Machine / Cell | CNC-9 |
Machine / Cell No. | CNC Section |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Machining Process & Inspection Method Wrong | Machining Process is ok But Inspection Method Wrong | X |
Man | Unskilled operator | As per Skilled Matrix Operator is skilled | O |
Tool | Wrong Tool Insert Use | Correct carbide Insert Facing and Turning Tool Use | O |
Material | Wrong Grade And other grade Material Use | Correct Grade F15.4-EN8D Material use . | O |
Method | Machine Condition Not OK | As per Daily Check sheet Machine Condition was ok but Stopper Not OK | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20Nos /Bin |
7. Root Cause Analysis (Occurance)
Why 1 | LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1 |
Why 2 | During piston side machining, the part was resting too deep in the CNC chuck |
Why 3 | CNC Resting stopper lock Nut Loose |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | CNC Resting stopper lock Nut Loose. |
Root Cause Analysis (Outflow)
Why 1 | LENGTH UNDERSIZE-T.LENGTH U/S SPE=173.30+/-0.20 OBS=172.1 |
Why 2 | Sampling measuring Frequency Very Low. |
Why 3 | Hourly 5 Nos Inspection By Inspector. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling measuring Frequency Very Low. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Arrange an additional lock nut to secure the resting stopper lock nut. | Production Head | 14/10/2024 | 14/10/2024 | Completed |
Outflow | The length measurement sampling frequency has been increased to 10 samples instead of 5. | Quality Head | 14/10/2024 | 14/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Length measurement sampling frequency has been increased to 10nos samples instead of 5.nos |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10Nos |
10. Evidance of Countermeasure
Occurance (Before) |
CNC Resting stopper lock Nut Loose. 1140_Occurance_Before.jpg |
Occurance (After) |
Arrange an additional lock nut to secure the resting stopper lock nut. 1140_Occurance_After.jpg |
Outflow (Before) |
Sampling measuring Frequency Very Low. 1140_Outflow_Before.docx |
Outflow (After) |
The length measurement sampling frequency has been increased to 10Nos samples instead of 5Nos. 1140_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Piston Rods |
12. Document Review
Documents | ControlPlan, PFMEA, JHCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |