QFR No - 7001067878
Defect Details
NC No. | 7001067878 |
NC Date | 25/10/2024 |
NC Submission Date | |
Part No. | F1DZ00902B |
Part Name | FORK BOLT K86A |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | MATERIAL DEFECT-Pitting mark |
1. Problem Description
Defect Description | Pitting marks (Material defect) |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1870 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2600
|
0
|
0
|
1500
|
0
|
4100
|
Check Qty |
2600
|
0
|
0
|
1500
|
0
|
4100
|
NG Qty |
1870
|
0
|
0
|
1400
|
0
|
3270
|
Scrap | 0 |
Rework | 3270 |
Under Deviation | 0 |
Containment Action |
---|
All pipeline material segregated |
3. Process Flow
Process Flow Description |
---|
RM inward-Paring and drilling-CNC setup-OD grinding-Milling-Roliing-Plating-FID-Packing and forwarding |
4. Process Details
Process / Operation | RM inwarding |
Outsource | Yes |
Machine / Cell | RM supplier |
Machine / Cell No. | RM supplier |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Material changed | Material found as per specification | O |
Man | manpower changed | manpower deployed as per skill matrix | O |
Machine | Operation missing | OD turning operation not done | X |
Method | part not clamp properly | part clamp properly | O |
Tool | Tool Change | no tool change | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Pitting Mark |
Why 2 | Pitting Mark at OD Collar |
Why 3 | OD turning Operation not done |
Why 4 | OD turning operation not available in program |
Why 5 | |
Root Cause (Occurance) | OD turning operation not available in program |
Root Cause Analysis (Outflow)
Why 1 | Pitting Mark |
Why 2 | Skip From inspection |
Why 3 | Inspector not aware about defect |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector not aware about defect |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Onjob Training given to inspector | Mr. Omkar Bhange | 28/10/2024 | 28/10/2024 | Completed |
Occurance | 1)OD turning Operation added in CNC program 2) RM Size increase by 0.05mm | Mr. Manoj Kadam | 28/10/2024 | 28/10/2024 | Completed |
Outflow | OPL displayed st final and machine stage | Omkar Bhange | 26/10/2024 | 26/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Started 100% inspection at final inspection |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
RM of OD 29.50 +0.1 mm were used for fork bolt K-86 1189_Occurance_Before.pdf |
Occurance (After) |
Now, RM of OD 29.55 +0.1 mm are using for fork bolt K-86 1189_Occurance_After.pdf |
Outflow (Before) |
Inspector were not aware about defect 1189_Outflow_Before.png |
Outflow (After) |
On job training given to the inspector 1189_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All fork bolt |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Material defect -Pitting mark |