QFR No - 7001083193
Defect Details
NC No. 7001083193
NC Date 19/12/2024
NC Submission Date
Part No. S2FF00802B
Part Name GAS CAP- K1 RSA GDC CANISTER
Supplier Name & Code 100827-SANJAY TECHNOPLAST PVT.LTD.
ETL Plant 1126-ETL Pantnagar
Defect Details DIMETER UNDERSIZE-DIA. 38.0 OD UNDERSIZE
 
1. Problem Description
Defect Description O/D 38.0 mm UNDERSIZE :- Gas Cap Side Leakage issue
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2700
Is Defect Repeatative? No
Defect Sketch / Photo r5lpxjqnsj3bzlhliwtydmnl.png
Supplier Communication Details
Quality Head Email ID qa.hodstplpn@sanjaygroup.in
Plant Head/CEO Email ID praveen.singh@sanjaygroup.in
MD Email ID accounts.pn@sanjaygroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3200
0
0
25000
0
28200
Check Qty
3200
0
0
25000
0
28200
NG Qty
2700
0
0
2000
0
4700
 
Scrap 4700
Rework 0
Under Deviation 0
Containment Action
1-100 % inspection done at Customer end . 2- Accumulated material inspection at STPL end . 3-OPL Display 4-Sampling inspection increase -
 
3. Process Flow
Process Flow Description
M Inspection-RM Storage-Pre-Heating-Inj. Moulding-Deflashing-PDI-Packing-Logistics
 
4. Process Details
Process / Operation Injection Moulding
Outsource Yes
Machine / Cell Moulding
Machine / Cell No. FM110
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineInjection holding time lessVerify with SPPS, Injection Holding time found lessO
MachineScrew Position LessVerify with SPPS material screw position found less due to srinkage obsevedO
MethodInspection check point not definedDia 38 +/-0.1 mm not aided in PDI ReportsO
MethodImproper slider matchingVisualX
ManUnskilled InspectorDedicate inspector is available for inspection as per skill levelX
MachineBarrel temprature lowVerify with SPPS Barrel temprature found lowO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Leakage issue Observed in Gas cap
Why 2 OD under size Specification -Dia 38 ±0.1 Observation -37.73 mm
Why 3 Injection holding time & screw position less
Why 4
Why 5
Root Cause (Occurance) Injection holding time & screw position less
 
Root Cause Analysis (Outflow)
Why 1 Leakage issue Observed in Gas cap
Why 2 Not deduct during Pre-dispatch Inspection
Why 3 Check Point was not defined in PDI inspection Check sheet for OD 38 ±0.1 mm
Why 4
Why 5
Root Cause (Outflow) Check Point was not defined in PDI inspection Check sheet for OD 38 ±0.1 mm .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1-Injection holding time increase 2-Barrel temprature increase 3-Injection Screw Position increaseMr .Jitendar10/01/202529/12/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Check Point Defined in Pre-Dispatch Inspection Reports for OD 38 ±0.1 mm 100 % inspection .
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
10. Evidance of Countermeasure
Occurance (Before) Unskilled Operator Unskilled Inspector
1282_Occurance_Before.pdf
Occurance (After) 1-Training Provided to Operators. 2-One Point Lesson Displayed
1282_Occurance_After.jpg
Outflow (Before) Injection holding time less Barrel temperature low Screw Position Less
1282_Outflow_Before.jpg
Outflow (After) 1-Injection holding time increase 2-Barrel temperature increase 3-Injection Screw Position increase
1282_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Gas Cap BS 4
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, JHCheckSheet, AuditCheckSheet, ProcessFlowChart, InspCheckSheet
Specify Other Document OPL ,OJT
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission