QFR No - 8000778361
Defect Details
NC No. 8000778361
NC Date 03/03/2022
NC Submission Date
Part No. 520MD19002
Part Name COMPRESSION SPRING ( 4 PLATE VAVE)
Supplier Name & Code 207123-NHK AUTOMOTIVE COMPONENTS
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details DIAMETER OVER SIZE-WIRE DIA 2.40 O/S UPTO 2.60MM
 
1. Problem Description
Defect Description Wire diameter observed 2.6 mm as against 2.4 mm
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID aamerkhan@nhkspring.co.in
Plant Head/CEO Email ID vrdhage@nhkspring.co.in
MD Email ID j.mizutani@nhkspringindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
0
15000
0
25000
Check Qty
10000
0
0
15000
0
25000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100% Mix up sorting done .
 
3. Process Flow
Process Flow Description
Coiling-Stress relieving-grinding-hoscoat -preinspection-painting oiling-100% Visual sorting-Packing
 
4. Process Details
Process / Operation Painting machine
Outsource No
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManChances of mix up at coilingVerified at coiling process, lot taken separately, no chance of mix up spring. fallen spring scrapX
MethodChances of Mix-up at Stress relieving processVerified at stress relieving process, lot taken separately, no chance of mix up spring. fallen sprX
MethodChances of Mix-up at Shot peening process.verified at Shot peening process, there is no possibility of mix-up spring as one batch taken separaX
Method1.Spring mix up painting process1.Painting process verify as spring remain at corner of painting trayO
ManChances of Mix-up at Grinding processverified at Grinding process, lot taken separately as per batch, No chance of mix up spring at GrindX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual checking
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Mix up spring found
Why 2 spring mix up at painting process
Why 3 Remain spring of previous lot at corner of painting tray got mix up in next lot.
Why 4 Remain spring not verified after completion of lot
Why 5 Remain spring checking requirement not identified in painting process
Root Cause (Occurance) Remain spring checking requirement not identified in painting process
 
Root Cause Analysis (Outflow)
Why 1 Mix up spring found
Why 2 spring not detected in visual sorting
Why 3 Both Ok & NG spring are similar looking
Why 4
Why 5
Root Cause (Outflow) Since ,spring not arrested in visual sorting as both spring are similar looking.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1.Now remain spring check requirement added in painting process.2)Remain spring check map made & displayed & to be monitored by remain spring check sheet after completion of every lotS F NEHRI03/10/2022Pending
Outflow1.100% Gauge sorting started to arrest mix up spring as there is difference between in ID of OK & NG part.(NG Part ID Is 13.50mm & OK part ID is 14.80mm)S F NEHRI03/10/2022Pending
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Gauge sorting started at detection side to arrest mix up spring
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Remain check map not available at painting process
2_Occurance_Before.pdf
Occurance (After) Remain check map displayed at painting process & remain spring check sheet provided
2_Occurance_After.pdf
Outflow (Before) Only visual sorting done
2_Outflow_Before.jpg
Outflow (After) Gauge sorting started to arrest mix up spring
2_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Horizontal deployment done at painting process for all ETL Parts.
 
12. Document Review
Documents WISOP
Specify Other Document No other document
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission What is your inspection method of 100% inspection not defined and how this going to detect the problem not confirm. Also cause side action not full proof.