QFR No - 8000779369
Defect Details
NC No. 8000779369
NC Date 10/03/2022
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details MIX UP OTHER MODEL-WRONG PART NOT USING K0PG REAR MODEL
 
1. Problem Description
Defect Description adjuster small size part mix up not using K0PG Rear model
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 8
Is Defect Repeatative? No
Defect Sketch / Photo y1hynmfxkooqo3rg1jwpcn4h.xlsx
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
1000
2000
3000
Check Qty
0
0
0
1000
2000
3000
NG Qty
0
0
0
1
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
100% MATERIAL CHECKED AT WIP AND FINISH GOOD .
 
3. Process Flow
Process Flow Description
PROCESS SEQUENCE CHART 10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 80 ID SIZING 90 SIDE GRINDING 100 BROACHING 110 HEAD GRINDING & BUFFING 120 OUTSIDE MOVEMENT FOR PLATING 130 STORAGE & RQC INSP. OF PLATED MATERIAL 140 FINAL INSPECTION 150 PACKING & DISPATCH
 
4. Process Details
Process / Operation 120 OUTSIDE MOVEMENT FOR PLATING
Outsource No
Machine / Cell DISPATCH FOR PLATING
Machine / Cell No. NA
5. Problem Analysis
-------
Type Possible Cause Fact Verification Jud
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Only sampling base
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 100 pcs
7. Root Cause Analysis (Occurance)
Why 1 Wrong model part dispatch to customer
Why 2 Plating done in wrong model part
Why 3 Wrong model part mix-up during dispatch time (Outsource plating)
Why 4 Only sampling Inspection done before dispatch to plating supplier for plating
Why 5
Root Cause (Occurance) Inspection system was not define before plating
 
Root Cause Analysis (Outflow)
Why 1 Wrong model part passed to customer
Why 2 Part could not detect during inspection time
Why 3 Same id spec in both part so part easily qualify in gauge during inspection
Why 4
Why 5
Root Cause (Outflow) Same id spec in both part so part easily qualify in gauge during inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowOne Point lesson displayed at PDI stageNice Team02/04/202201/04/2022Completed
Occurance100% visual inspection started before dispatch to plating (outsource)Nice Team01/04/202201/04/2022Completed
OutflowTraining provided to inspector for both similar partNice Team02/04/202201/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection started before dispatch to plating (outsource)
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Only sapling inspection being done
13_Occurance_Before.pdf
Occurance (After) Training provided to all concern person about visual inspection .
13_Occurance_After.pdf
Outflow (Before) No any OPL
13_Outflow_Before.pdf
Outflow (After) OPL made and displayed
13_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents InspCheckSheet
Specify Other Document Inspection added
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission reviewed 10000 no mix up issue